GTG incident on 2015-10-24 — MI

Operator
Consumers Energy Co
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,921
Incident datetime
2015-10-24 11:55
Report number
Location
MI
Narrative
At approximately 11:55 on saturday, october 24, 2015 consumers energy gas control was notified by a landowner of a possible gas leak at the cranberry storage field. A gas system mechanic (gsm) was dispatch and arrived on-site at 12:23 and identified blowing gas on lateral 60 west. The leak location was approximately 1750 feet north of well 367. Lateral 60 west is a 6 inch pipeline (approximately 11/2 miles long) located in consumers energy's cranberry storage field, marion, michigan (missaukee county) the gsm implemented the standard precautionary lock out tag out process, isolating and shutting down lateral 60 west and barricaded the location until further investigation could be performed. The pipeline was shut down at approximately 12:31. On tueday, november 3, 2015 a 4 foot section of pipeline was cut out and a oval hole approximately .25 x .50 was discovered. The leak was visually examined and preliminary analysis identified corrosion as a possible leak source. The gas loss calculation was determined based on the following information: lateral 60 west was placed back into service on october 7, 2015. The leak was identified and the pipeline was isolated and shut down on october 24, 2015 approximately 36 minutes following notification. A visual inspection was performed by operations personnel when the pipeline was placed back into service, however no additional inspections/patrols were conducted. Because no additional leak inspection was performed during this period, consumers energy opted to calculate the hours from the date the line was placed back in service on october 7th until the leak was discovered and the lateral shut-down resulting in a gas loss of approximately 37mmcf. The gas loss calculation based on notification and isolation and shut down would have resulted in a gas loss calculation of less than 1mmcf. The damaged section of the pipeline was transported to the consumers energy trail street laboratory for further examination. Laboratory analysis confirmed the leak was a result of a localized corrosion pit on the pipe id. The mic testing performed on sludge extracted from the pipeline indicates microbiological influence corrosion (mic) may have caused or contributed to the failure. Lateral 60 west remains shut-in and scheduled for replacement both lateral 60 east and west will be eliminated and replaced with one lateral in summer 2016.
Detailed record list
Report Received Date
2015-11-24 00:00:00
Iyear
2015
Report Number
20150140
Supplemental Number
17172
Report Type
Supplemental Final
Operator Id
Name
Consumers Energy Co
Operator Street Address
One Energy Plaza
Operator City Name
Jackson
Operator State Abbreviation
MI
Operator Postal Code
49201
Local Datetime
2015-10-24 11:55:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-11-13 10:29:00
Commodity Released Type
Natural Gas
Unintentional Release
37025
Intentional Release
91.5
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-24 12:31:00
Still Shutdown Ind
Yes
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-10-24 11:55:00
On Site Datetime
2015-10-24 12:23:00
On Off Shore
Onshore
Onshore State Abbreviation
Mi
Onshore Postal Code
49665
Onshore City Name
Marion
Onshore County Name
Missaukee
Designated Location
Survey Station No.
Designated Name
Station 60 W
Pipe Fac Name
Cranberry Lake Storage Field
Segment Name
Lateral 60 West
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Belowground Storage, Including Associated Equipment And Piping
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
35000
Pipe Specification
Api5l
Pipe Seam Type
Longitudinal Erw - Unknown Frequency
Pipe Manufacturer
Youngtown Sheet & Tube
Pipe Coating Type
Other
Pipe Coating Details
Black Wrap With Light Brown Outer Layer, No Abestos Fibers
Installation Year
1957
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Oval Hole Appr .25 X .50
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
117
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
277728
Est Cost Intentional Release
682
Est Cost Prop Damage
10921
Est Cost Emergency
494
Est Cost Other
3127
Est Cost Other Details
Lab Analysis
Prpty
292952
Accident Psig
709
Mop Psig
800
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The facility was not monitored by a controller at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Mic Testing
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2005
Other Tool
Micro Vertiline Tool
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1999
Hydrtst Most Rcnt Pressure
1241
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C******* K***
Preparer Title
Senior Engineering Technical Analyst Ii
Preparer Email
C************@c********.com
Preparer Telephone
734-513-6256
Authorizer Name
A***** L* W***
Authorizer Title
Gas Regulatory Services Lead
Authorizer Telephone
517-545-8746
Authorizer Email
A**********@c********
Narrative
At approximately 11:55 on saturday, october 24, 2015 consumers energy gas control was notified by a landowner of a possible gas leak at the cranberry storage field. A gas system mechanic (gsm) was dispatch and arrived on-site at 12:23 and identified blowing gas on lateral 60 west. The leak location was approximately 1750 feet north of well 367. Lateral 60 west is a 6 inch pipeline (approximately 11/2 miles long) located in consumers energy's cranberry storage field, marion, michigan (missaukee county) the gsm implemented the standard precautionary lock out tag out process, isolating and shutting down lateral 60 west and barricaded the location until further investigation could be performed. The pipeline was shut down at approximately 12:31. On tueday, november 3, 2015 a 4 foot section of pipeline was cut out and a oval hole approximately .25 x .50 was discovered. The leak was visually examined and preliminary analysis identified corrosion as a possible leak source. The gas loss calculation was determined based on the following information: lateral 60 west was placed back into service on october 7, 2015. The leak was identified and the pipeline was isolated and shut down on october 24, 2015 approximately 36 minutes following notification. A visual inspection was performed by operations personnel when the pipeline was placed back into service, however no additional inspections/patrols were conducted. Because no additional leak inspection was performed during this period, consumers energy opted to calculate the hours from the date the line was placed back in service on october 7th until the leak was discovered and the lateral shut-down resulting in a gas loss of approximately 37mmcf. The gas loss calculation based on notification and isolation and shut down would have resulted in a gas loss calculation of less than 1mmcf. The damaged section of the pipeline was transported to the consumers energy trail street laboratory for further examination. Laboratory analysis confirmed the leak was a result of a localized corrosion pit on the pipe id. The mic testing performed on sludge extracted from the pipeline indicates microbiological influence corrosion (mic) may have caused or contributed to the failure. Lateral 60 west remains shut-in and scheduled for replacement both lateral 60 east and west will be eliminated and replaced with one lateral in summer 2016.
Report Received Date 2015-11-24 00:00:00
Iyear 2015
Report Number 20150140
Supplemental Number 17172
Report Type Supplemental Final
Operator Id 2748 PHMSA Enforcement
Name Consumers Energy Co
Operator Street Address One Energy Plaza
Operator City Name Jackson
Operator State Abbreviation MI
Operator Postal Code 49201
Local Datetime 2015-10-24 11:55:00
Location Latitude 44.161972 Google Maps OpenStreetMap
Location Longitude -85.006155 Google Maps OpenStreetMap
Nrc Rpt Num 1133332 NRC Report How to search
Nrc Rpt Datetime 2015-11-13 10:29:00
Commodity Released Type Natural Gas
Unintentional Release 37025
Intentional Release 91.5
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-24 12:31:00
Still Shutdown Ind Yes
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-10-24 11:55:00
On Site Datetime 2015-10-24 12:23:00
On Off Shore Onshore
Onshore State Abbreviation Mi
Onshore Postal Code 49665
Onshore City Name Marion
Onshore County Name Missaukee
Designated Location Survey Station No.
Designated Name Station 60 W
Pipe Fac Name Cranberry Lake Storage Field
Segment Name Lateral 60 West
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
System Part Involved Belowground Storage, Including Associated Equipment And Piping
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys 35000
Pipe Specification Api5l
Pipe Seam Type Longitudinal Erw - Unknown Frequency
Pipe Manufacturer Youngtown Sheet & Tube
Pipe Coating Type Other
Pipe Coating Details Black Wrap With Light Brown Outer Layer, No Abestos Fibers
Installation Year 1957
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Oval Hole Appr .25 X .50
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 117
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 277728
Est Cost Intentional Release 682
Est Cost Prop Damage 10921
Est Cost Emergency 494
Est Cost Other 3127
Est Cost Other Details Lab Analysis
Prpty 292952
Accident Psig 709
Mop Psig 800
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The facility was not monitored by a controller at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Mic Testing
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2005
Other Tool Micro Vertiline Tool
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1999
Hydrtst Most Rcnt Pressure 1241
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C******* K***
Preparer Title Senior Engineering Technical Analyst Ii
Preparer Email C************@c********.com
Preparer Telephone 734-513-6256
Authorizer Name A***** L* W***
Authorizer Title Gas Regulatory Services Lead
Authorizer Telephone 517-545-8746
Authorizer Email A**********@c********
Narrative At approximately 11:55 on saturday, october 24, 2015 consumers energy gas control was notified by a landowner of a possible gas leak at the cranberry storage field. A gas system mechanic (gsm) was dispatch and arrived on-site at 12:23 and identified blowing gas on lateral 60 west. The leak location was approximately 1750 feet north of well 367. Lateral 60 west is a 6 inch pipeline (approximately 11/2 miles long) located in consumers energy's cranberry storage field, marion, michigan (missaukee county) the gsm implemented the standard precautionary lock out tag out process, isolating and shutting down lateral 60 west and barricaded the location until further investigation could be performed. The pipeline was shut down at approximately 12:31. On tueday, november 3, 2015 a 4 foot section of pipeline was cut out and a oval hole approximately .25 x .50 was discovered. The leak was visually examined and preliminary analysis identified corrosion as a possible leak source. The gas loss calculation was determined based on the following information: lateral 60 west was placed back into service on october 7, 2015. The leak was identified and the pipeline was isolated and shut down on october 24, 2015 approximately 36 minutes following notification. A visual inspection was performed by operations personnel when the pipeline was placed back into service, however no additional inspections/patrols were conducted. Because no additional leak inspection was performed during this period, consumers energy opted to calculate the hours from the date the line was placed back in service on october 7th until the leak was discovered and the lateral shut-down resulting in a gas loss of approximately 37mmcf. The gas loss calculation based on notification and isolation and shut down would have resulted in a gas loss calculation of less than 1mmcf. The damaged section of the pipeline was transported to the consumers energy trail street laboratory for further examination. Laboratory analysis confirmed the leak was a result of a localized corrosion pit on the pipe id. The mic testing performed on sludge extracted from the pipeline indicates microbiological influence corrosion (mic) may have caused or contributed to the failure. Lateral 60 west remains shut-in and scheduled for replacement both lateral 60 east and west will be eliminated and replaced with one lateral in summer 2016.

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