GTG incident on 2015-10-23 — CA

Operator
Pacific Gas & Electric Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300,000
Incident datetime
2015-10-23 11:23
Report number
Location
CA
Narrative
On october 23, 2015 at 1123 hours, pg&e was notified of blowing gas in a field near 5430 putah creek rd. Dixon, solano county. Pg&e gas service representative arrived on site at 1206 hours and a gas pipeline operations and maintenance (gpom) crew at 1245 hours. It was determined that transmission line l-150 at milepoint (mp) 7.23 had been struck by a ripper being pulled in an agricultural field by a bulldozer being operated by nichelini construction. The excavator held a USA ticket #490858 and the pipeline had been properly marked prior to the incident. The operator had made numerous passes over the pipeline but failed to raise the ripper during the pass which struck the pipe. The depth, at which the line was damaged, was approximately 39 inches below the surface of the soil. No injuries, fatalities, or ignition. Damage to the transmission pipeline, including repairs is approximately $300,000. Pg&e secured the area and closed mainline valve v-9.7 at 1504 hours and 90% closed v-5.96 at 1617 hours in order to keep a positive pressure in the shut-in section of pipeline. The flow of gas was completely stopped at 1849 hours. Repairs on the pipeline were completed on 10/23/15 at 2238 hours and the pipeline was restored to normal operation on 10/25/15 at 0140 hours. Gas service to the customers was restored by 10/26/15 at 1330 hours.
Detailed record list
Report Received Date
2015-11-24 00:00:00
Iyear
2015
Report Number
20150139
Supplemental Number
16930
Report Type
Original Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2015-10-23 11:23:00
Location Latitude
Location Longitude
-121.8908531
Nrc Rpt Num
Nrc Rpt Datetime
2015-10-23 14:22:00
Commodity Released Type
Natural Gas
Unintentional Release
2655
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-23 18:49:00
Restart Datetime
2015-10-25 01:40:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-10-23 11:23:00
On Site Datetime
2015-10-23 12:06:00
On Off Shore
Onshore
Onshore State Abbreviation
Ca
Onshore Postal Code
95620
Onshore City Name
Dixon
Onshore County Name
Solano
Designated Location
Milepost
Designated Name
Mile Point
Pipe Fac Name
L-150
Segment Name
Mp 7.23
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
39
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.28
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Epoxy
Installation Year
1949
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
6.6
Puncture Circum
20.8
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
52
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
0
Est Cost Intentional Release
0
Est Cost Prop Damage
300000
Est Cost Emergency
0
Est Cost Other
0
Prpty
300000
Accident Psig
118
Mop Psig
125
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
19483
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Scada-related equipment operated as intended
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
Yes
One Call Ticket Num
490858
One Call Center Name
Usa North 811
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
1470
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
S****** R****
Preparer Title
Compliance Engineer
Preparer Email
S***@p**.com
Preparer Telephone
925-328-6107
Authorizer Name
L**** D*******
Authorizer Title
Manager Of Regulatory Compliance
Authorizer Telephone
925-328-5756
Authorizer Email
L***@p**.com
Narrative
On october 23, 2015 at 1123 hours, pg&e was notified of blowing gas in a field near 5430 putah creek rd. Dixon, solano county. Pg&e gas service representative arrived on site at 1206 hours and a gas pipeline operations and maintenance (gpom) crew at 1245 hours. It was determined that transmission line l-150 at milepoint (mp) 7.23 had been struck by a ripper being pulled in an agricultural field by a bulldozer being operated by nichelini construction. The excavator held a USA ticket #490858 and the pipeline had been properly marked prior to the incident. The operator had made numerous passes over the pipeline but failed to raise the ripper during the pass which struck the pipe. The depth, at which the line was damaged, was approximately 39 inches below the surface of the soil. No injuries, fatalities, or ignition. Damage to the transmission pipeline, including repairs is approximately $300,000. Pg&e secured the area and closed mainline valve v-9.7 at 1504 hours and 90% closed v-5.96 at 1617 hours in order to keep a positive pressure in the shut-in section of pipeline. The flow of gas was completely stopped at 1849 hours. Repairs on the pipeline were completed on 10/23/15 at 2238 hours and the pipeline was restored to normal operation on 10/25/15 at 0140 hours. Gas service to the customers was restored by 10/26/15 at 1330 hours.
Report Received Date 2015-11-24 00:00:00
Iyear 2015
Report Number 20150139
Supplemental Number 16930
Report Type Original Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2015-10-23 11:23:00
Location Latitude 38.5140764 Google Maps OpenStreetMap
Location Longitude -121.8908531 Google Maps OpenStreetMap
Nrc Rpt Num 1131545 NRC Report How to search
Nrc Rpt Datetime 2015-10-23 14:22:00
Commodity Released Type Natural Gas
Unintentional Release 2655
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-23 18:49:00
Restart Datetime 2015-10-25 01:40:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-10-23 11:23:00
On Site Datetime 2015-10-23 12:06:00
On Off Shore Onshore
Onshore State Abbreviation Ca
Onshore Postal Code 95620
Onshore City Name Dixon
Onshore County Name Solano
Designated Location Milepost
Designated Name Mile Point
Pipe Fac Name L-150
Segment Name Mp 7.23
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 39
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.28
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Epoxy
Installation Year 1949
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 6.6
Puncture Circum 20.8
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 52
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 0
Est Cost Intentional Release 0
Est Cost Prop Damage 300000
Est Cost Emergency 0
Est Cost Other 0
Prpty 300000
Accident Psig 118
Mop Psig 125
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 19483
Internal Inspection Ind No
Other Restrictions Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Scada-related equipment operated as intended
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind Yes
One Call Ticket Num 490858
One Call Center Name Usa North 811
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 1470
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name S****** R****
Preparer Title Compliance Engineer
Preparer Email S***@p**.com
Preparer Telephone 925-328-6107
Authorizer Name L**** D*******
Authorizer Title Manager Of Regulatory Compliance
Authorizer Telephone 925-328-5756
Authorizer Email L***@p**.com
Narrative On october 23, 2015 at 1123 hours, pg&e was notified of blowing gas in a field near 5430 putah creek rd. Dixon, solano county. Pg&e gas service representative arrived on site at 1206 hours and a gas pipeline operations and maintenance (gpom) crew at 1245 hours. It was determined that transmission line l-150 at milepoint (mp) 7.23 had been struck by a ripper being pulled in an agricultural field by a bulldozer being operated by nichelini construction. The excavator held a USA ticket #490858 and the pipeline had been properly marked prior to the incident. The operator had made numerous passes over the pipeline but failed to raise the ripper during the pass which struck the pipe. The depth, at which the line was damaged, was approximately 39 inches below the surface of the soil. No injuries, fatalities, or ignition. Damage to the transmission pipeline, including repairs is approximately $300,000. Pg&e secured the area and closed mainline valve v-9.7 at 1504 hours and 90% closed v-5.96 at 1617 hours in order to keep a positive pressure in the shut-in section of pipeline. The flow of gas was completely stopped at 1849 hours. Repairs on the pipeline were completed on 10/23/15 at 2238 hours and the pipeline was restored to normal operation on 10/25/15 at 0140 hours. Gas service to the customers was restored by 10/26/15 at 1330 hours.

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