GTG incident on 2015-08-14 — NC

Operator
Pitt Landfill Gas, Llc
Cause
Equipment Failure
Commodity
Landfill Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2015-08-14 08:00
Report number
Location
NC
Narrative
Line is a low pressure (6 psig) line that transmits landfill gas (lfg) approxiamtelyk 11,000 feet from the landfill to a hospital boiler room. Evidence of leak was found during a line walk in q4 2014. Several attempts were made in q1 of 2015 to find and repair the leak. Leak was found in q3 2015 under sidewalk immediately adjacent to busy roadway. Leak was repaired when found. Leak appears to have been from a previous repair (hdpe electrofusion fitting was found to be leaking).
Detailed record list
Report Received Date
2015-11-04 00:00:00
Iyear
2015
Report Number
20150130
Supplemental Number
17576
Report Type
Supplemental
Operator Id
Name
Pitt Landfill Gas, Llc
Operator Street Address
10600 Nations Ford Rd Suite 150
Operator City Name
Charlotte
Operator State Abbreviation
NC
Operator Postal Code
28273
Local Datetime
2015-08-14 08:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Notification Not Required
Commodity Released Type
Landfill Gas
Unintentional Release
390
Intentional Release
9
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-21 00:00:00
Restart Datetime
2015-08-21 08:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-08-14 08:00:00
On Site Datetime
2015-08-21 00:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Nc
Onshore Postal Code
27834
Onshore City Name
Greenville
Onshore County Name
Pitt
Designated Location
Milepost
Designated Name
1.56 Mile Mar
Pipe Fac Name
Pitt Landfill Gas
Segment Name
Pitt Landfill Gas
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Repair Sleeve Or Clamp
Installation Year
1998
Material Involved
Plastic
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 3 Location
Could Be Hca
No
Pir Radius
65
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1100
Est Cost Intentional Release
5
Est Cost Prop Damage
25000
Est Cost Emergency
0
Est Cost Other
0
Prpty
26105
Accident Psig
6
Mop Psig
60
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
10900
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Plastic Pipe, No Access Except At Ends
Pipeline Function
Transmission System
Scada In Place Ind
No
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
Failure Of Electrofusion Joint Where Pipe Was Connected.
Additional Installation Ind
Yes
Preparer Name
T****** L K*******
Preparer Title
Ehs And Engineering Director
Preparer Email
T***************@l************.com
Preparer Telephone
7048448990
Preparer Fax
7048448994
Authorizer Name
W****** P* B******
Authorizer Title
Manager Of The Llc
Authorizer Telephone
7048448990
Authorizer Email
W**************@l************.com
Narrative
Line is a low pressure (6 psig) line that transmits landfill gas (lfg) approxiamtelyk 11,000 feet from the landfill to a hospital boiler room. Evidence of leak was found during a line walk in q4 2014. Several attempts were made in q1 of 2015 to find and repair the leak. Leak was found in q3 2015 under sidewalk immediately adjacent to busy roadway. Leak was repaired when found. Leak appears to have been from a previous repair (hdpe electrofusion fitting was found to be leaking).
Report Received Date 2015-11-04 00:00:00
Iyear 2015
Report Number 20150130
Supplemental Number 17576
Report Type Supplemental
Operator Id 32037 PHMSA Enforcement
Name Pitt Landfill Gas, Llc
Operator Street Address 10600 Nations Ford Rd Suite 150
Operator City Name Charlotte
Operator State Abbreviation NC
Operator Postal Code 28273
Local Datetime 2015-08-14 08:00:00
Location Latitude 35.605267 Google Maps OpenStreetMap
Location Longitude -77.411687 Google Maps OpenStreetMap
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Commodity Released Type Landfill Gas
Unintentional Release 390
Intentional Release 9
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-21 00:00:00
Restart Datetime 2015-08-21 08:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-08-14 08:00:00
On Site Datetime 2015-08-21 00:00:00
On Off Shore Onshore
Onshore State Abbreviation Nc
Onshore Postal Code 27834
Onshore City Name Greenville
Onshore County Name Pitt
Designated Location Milepost
Designated Name 1.56 Mile Mar
Pipe Fac Name Pitt Landfill Gas
Segment Name Pitt Landfill Gas
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Repair Sleeve Or Clamp
Installation Year 1998
Material Involved Plastic
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 3 Location
Could Be Hca No
Pir Radius 65
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1100
Est Cost Intentional Release 5
Est Cost Prop Damage 25000
Est Cost Emergency 0
Est Cost Other 0
Prpty 26105
Accident Psig 6
Mop Psig 60
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 10900
Internal Inspection Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Other Complications Ind Yes
Inspect Comp Details Plastic Pipe, No Access Except At Ends
Pipeline Function Transmission System
Scada In Place Ind No
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Contractor Working For The Operator
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Other
Other Non Threaded Details Failure Of Electrofusion Joint Where Pipe Was Connected.
Additional Installation Ind Yes
Preparer Name T****** L K*******
Preparer Title Ehs And Engineering Director
Preparer Email T***************@l************.com
Preparer Telephone 7048448990
Preparer Fax 7048448994
Authorizer Name W****** P* B******
Authorizer Title Manager Of The Llc
Authorizer Telephone 7048448990
Authorizer Email W**************@l************.com
Narrative Line is a low pressure (6 psig) line that transmits landfill gas (lfg) approxiamtelyk 11,000 feet from the landfill to a hospital boiler room. Evidence of leak was found during a line walk in q4 2014. Several attempts were made in q1 of 2015 to find and repair the leak. Leak was found in q3 2015 under sidewalk immediately adjacent to busy roadway. Leak was repaired when found. Leak appears to have been from a previous repair (hdpe electrofusion fitting was found to be leaking).

All rights reserved. Copyright © by ClearPHMSA