GTG incident on 2015-10-01 — OK

Operator
Oneok Westex Transmission, Llc
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200,000
Incident datetime
2015-10-01 15:05
Report number
Location
OK
Narrative
On october 1, 2015, the operating pressure on parallel lines 800-000 and 801-000 appeared to the control room operators to be lower than expected. Field operations personnel confirmed gas venting to atmosphere on line 800-000. The pipeline is in a low wet area that has prevented close examination of the failure beyond a single photograph of the pipe before being covered by ground water. Line 800-000 will remain out of service until a repair method has been determined. Line 801-000 will remain in service. Supplemental - the failure site became accessible and the pipeline was repaired by installing a cylinder of tested pipe. External corrosion was confirmed to be the cause of the failure.
Detailed record list
Report Received Date
2015-10-30 00:00:00
Iyear
2015
Report Number
20150129
Supplemental Number
17233
Report Type
Supplemental Final
Operator Id
Name
Oneok Westex Transmission, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-10-01 15:05:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-10-01 15:56:00
Commodity Released Type
Natural Gas
Unintentional Release
3624
Intentional Release
452
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-01 16:08:00
Still Shutdown Ind
Yes
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-10-01 15:05:00
On Site Datetime
2015-10-01 15:26:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79782
Onshore City Name
Not Within A Municipality
Onshore County Name
Martin
Designated Location
Milepost
Designated Name
54.00
Pipe Fac Name
800-000
Segment Name
800-000
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
35
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.22
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Lap Welded
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Coal Tar
Installation Year
1930
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
4 Inch Dia Corroded Area
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
115
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
10292
Est Cost Intentional Release
1284
Est Cost Prop Damage
200000
Est Cost Emergency
1000
Est Cost Other
0
Prpty
212576
Accident Psig
350
Mop Psig
428
Mop Cfr Section
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
51744
Internal Inspection Ind
No
Diameter Change Ind
Yes
Unsuitable Mainline Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Controller
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Correct response by control room operators to the situation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2015
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1956
Hydrtst Most Rcnt Pressure
420
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
P****** V******
Preparer Title
Manager Regulatory Compliance
Preparer Email
P**********@o****.com
Preparer Telephone
918-588-7734
Preparer Fax
918-5915032
Authorizer Name
W** D*****
Authorizer Title
Vp Natural Gas Pipeline Operations
Authorizer Telephone
918-588-7424
Authorizer Email
W************@o****.com
Narrative
On october 1, 2015, the operating pressure on parallel lines 800-000 and 801-000 appeared to the control room operators to be lower than expected. Field operations personnel confirmed gas venting to atmosphere on line 800-000. The pipeline is in a low wet area that has prevented close examination of the failure beyond a single photograph of the pipe before being covered by ground water. Line 800-000 will remain out of service until a repair method has been determined. Line 801-000 will remain in service. Supplemental - the failure site became accessible and the pipeline was repaired by installing a cylinder of tested pipe. External corrosion was confirmed to be the cause of the failure.
Report Received Date 2015-10-30 00:00:00
Iyear 2015
Report Number 20150129
Supplemental Number 17233
Report Type Supplemental Final
Operator Id 31531 PHMSA Enforcement
Name Oneok Westex Transmission, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-10-01 15:05:00
Location Latitude 32.305 Google Maps OpenStreetMap
Location Longitude -101.7102 Google Maps OpenStreetMap
Nrc Rpt Num 1129881 NRC Report How to search
Nrc Rpt Datetime 2015-10-01 15:56:00
Commodity Released Type Natural Gas
Unintentional Release 3624
Intentional Release 452
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-01 16:08:00
Still Shutdown Ind Yes
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-10-01 15:05:00
On Site Datetime 2015-10-01 15:26:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 79782
Onshore City Name Not Within A Municipality
Onshore County Name Martin
Designated Location Milepost
Designated Name 54.00
Pipe Fac Name 800-000
Segment Name 800-000
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 35
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.22
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Lap Welded
Pipe Manufacturer Republic Steel
Pipe Coating Type Coal Tar
Installation Year 1930
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other 4 Inch Dia Corroded Area
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 115
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 10292
Est Cost Intentional Release 1284
Est Cost Prop Damage 200000
Est Cost Emergency 1000
Est Cost Other 0
Prpty 212576
Accident Psig 350
Mop Psig 428
Mop Cfr Section 192.619(C) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 51744
Internal Inspection Ind No
Diameter Change Ind Yes
Unsuitable Mainline Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Controller
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Correct response by control room operators to the situation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2015
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1956
Hydrtst Most Rcnt Pressure 420
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name P****** V******
Preparer Title Manager Regulatory Compliance
Preparer Email P**********@o****.com
Preparer Telephone 918-588-7734
Preparer Fax 918-5915032
Authorizer Name W** D*****
Authorizer Title Vp Natural Gas Pipeline Operations
Authorizer Telephone 918-588-7424
Authorizer Email W************@o****.com
Narrative On october 1, 2015, the operating pressure on parallel lines 800-000 and 801-000 appeared to the control room operators to be lower than expected. Field operations personnel confirmed gas venting to atmosphere on line 800-000. The pipeline is in a low wet area that has prevented close examination of the failure beyond a single photograph of the pipe before being covered by ground water. Line 800-000 will remain out of service until a repair method has been determined. Line 801-000 will remain in service. Supplemental - the failure site became accessible and the pipeline was repaired by installing a cylinder of tested pipe. External corrosion was confirmed to be the cause of the failure.

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