GTG incident on 2015-10-10 — OK

Operator
Transcontinental Gas Pipe Line Company
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-10-10 08:47
Report number
Location
OK
Narrative
Due to the location of a valve on a mainline transmission system an attached valve grease line had to be extended. A function of the modification process included cutting the grease line. When the grease line was cut an internal valve component failed allowing gas to escape, the transmission line segment was isolated and the grease line was repaired with a coupling. After the valve grease line was repaired the transmission line segment was pressured up and put back in service.
Detailed record list
Report Received Date
2015-10-28 00:00:00
Iyear
2015
Report Number
20150127
Supplemental Number
16914
Report Type
Supplemental Final
Operator Id
Name
Transcontinental Gas Pipe Line Company
Operator Street Address
One Williams Center Md 43-4
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2015-10-10 08:15:00
Location Latitude
Location Longitude
-74.68269956
Nrc Rpt Num
Nrc Rpt Datetime
2015-10-10 09:15:00
Commodity Released Type
Natural Gas
Unintentional Release
6271
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-10 11:20:00
Restart Datetime
2015-10-10 17:14:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-10-10 08:47:00
On Site Datetime
2015-10-10 09:40:00
On Off Shore
Onshore
Onshore State Abbreviation
Nj
Onshore Postal Code
08540
Onshore City Name
Princeton
Onshore County Name
Mecer
Designated Location
Milepost
Designated Name
1776.75
Pipe Fac Name
Mainline B Coventry Farms
Segment Name
Mlv J951
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Tubing
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Operator Technicians Intentionally Cut A Valve Grease Line During A Modification Process. An Internal Valve Component (Check Valve) Failed Allowing Gas To Escape.
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
15700
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
0
Prpty
15700
Accident Psig
721
Mop Psig
800
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Length Segment Isolated
17688
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
A Modification To A Valve Involved Cutting A Valve Grease Line. The Valve Body Was Blown Down Of All Gas But An Internal Check Valve Failed And Allowed Gas To Escape From The Grease Line. The Affected Gas Line Segment Was Isolated Until The Line Was Completely Blown Down, The Grease Line Was Repaired And The Affected Gas Line Segment Was Pressured Up And Put Back Into Service.
Preparer Name
J***** L****
Preparer Title
Regulatory Compliance Specialist
Preparer Email
J***********@w*******.com
Preparer Telephone
7132152995
Preparer Fax
7132152000
Authorizer Name
M**** S****
Authorizer Title
Manager Pipeline Safety
Authorizer Telephone
7132152111
Authorizer Email
M**********@w*******.com
Narrative
Due to the location of a valve on a mainline transmission system an attached valve grease line had to be extended. A function of the modification process included cutting the grease line. When the grease line was cut an internal valve component failed allowing gas to escape, the transmission line segment was isolated and the grease line was repaired with a coupling. After the valve grease line was repaired the transmission line segment was pressured up and put back in service.
Report Received Date 2015-10-28 00:00:00
Iyear 2015
Report Number 20150127
Supplemental Number 16914
Report Type Supplemental Final
Operator Id 19570 PHMSA Enforcement
Name Transcontinental Gas Pipe Line Company
Operator Street Address One Williams Center Md 43-4
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2015-10-10 08:15:00
Location Latitude 40.36413118 Google Maps OpenStreetMap
Location Longitude -74.68269956 Google Maps OpenStreetMap
Nrc Rpt Num 1130535 NRC Report How to search
Nrc Rpt Datetime 2015-10-10 09:15:00
Commodity Released Type Natural Gas
Unintentional Release 6271
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-10 11:20:00
Restart Datetime 2015-10-10 17:14:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-10-10 08:47:00
On Site Datetime 2015-10-10 09:40:00
On Off Shore Onshore
Onshore State Abbreviation Nj
Onshore Postal Code 08540
Onshore City Name Princeton
Onshore County Name Mecer
Designated Location Milepost
Designated Name 1776.75
Pipe Fac Name Mainline B Coventry Farms
Segment Name Mlv J951
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Tubing
Installation Year 2015
Material Involved Carbon Steel
Release Type Other
Release Type Details Operator Technicians Intentionally Cut A Valve Grease Line During A Modification Process. An Internal Valve Component (Check Valve) Failed Allowing Gas To Escape.
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 15700
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 0
Prpty 15700
Accident Psig 721
Mop Psig 800
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Length Segment Isolated 17688
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details A Modification To A Valve Involved Cutting A Valve Grease Line. The Valve Body Was Blown Down Of All Gas But An Internal Check Valve Failed And Allowed Gas To Escape From The Grease Line. The Affected Gas Line Segment Was Isolated Until The Line Was Completely Blown Down, The Grease Line Was Repaired And The Affected Gas Line Segment Was Pressured Up And Put Back Into Service.
Preparer Name J***** L****
Preparer Title Regulatory Compliance Specialist
Preparer Email J***********@w*******.com
Preparer Telephone 7132152995
Preparer Fax 7132152000
Authorizer Name M**** S****
Authorizer Title Manager Pipeline Safety
Authorizer Telephone 7132152111
Authorizer Email M**********@w*******.com
Narrative Due to the location of a valve on a mainline transmission system an attached valve grease line had to be extended. A function of the modification process included cutting the grease line. When the grease line was cut an internal valve component failed allowing gas to escape, the transmission line segment was isolated and the grease line was repaired with a coupling. After the valve grease line was repaired the transmission line segment was pressured up and put back in service.

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