Incident details
Operator, cause, commodity and consequences with raw source fields.
GTG incident on 2015-09-17 — TX
Operator
Kinetica Energy Express Llc
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$250,000
Incident datetime
2015-09-17 17:45
Report number
Location
TX
Narrative
On 9/17, fieldwood field supply boat observed a leak on kinetica's wc 68cg platform. Kinetica personnel dispatched and confirmed leak on the 20" riser at the +3' elevation. Kinetica personnel closed block valve on the platform to isolate leak from all production. Kinetica land personnel dispatched to close block valve located onshore to completely isolate pipeline. Kinetica began obtaining necessary blowdown/flare equipment in order to evacuate pressure from line. On 9/23, while equipment was being set up to prepare for evacuation of line, condensate began to mist from the leak location causing a slight silvery sheen. Blowdown/flaring of gas from the line began at noon on 9/23 (675psig). Misting and sheen continued until pressure was reduced to 78psig on the morning of 9/24. Jack-up boat and divers were located and dispatched to wc 68cg platform to evaluate leak. Due to location of leak at the +3' elevation on riser, work had to be performed during periods of calm seas. On 10/10, kinetica contractor completed the repair. On 10/11, pipeline was pressured-up to 300psig. Kinetica personnel discovered repair location was leaking. Block valve on platform was closed to once again isolate production. Pipeline evacuated of pressure. Vessel and contractor located and dispatched to location to initiate repairs. Supplemental report will be prepared and submitted upon completion of repair and placement of pipeline back into service.
Detailed record list
Report Received Date
2015-10-16 00:00:00
Iyear
2015
Report Number
20150125
Supplemental Number
16937
Report Type
Supplemental Final
Operator Id
38987
Name
Kinetica Energy Express Llc
Operator Street Address
1001 Mckinney Street, Suite 900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-09-17 17:45:00
Location Latitude
29.632371
Location Longitude
-93.038343
Nrc Rpt Num
1128765
Nrc Rpt Datetime
2015-09-17 18:30:00
Commodity Released Type
Natural Gas
Unintentional Release
260
Intentional Release
6900
Accompanying Liquid
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-09-17 18:53:00
Restart Datetime
2015-11-04 16:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-09-17 17:45:00
On Site Datetime
2015-09-17 18:15:00
On Off Shore
Offshore
Off Water Depth
33
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
West Cameron
Off Ocs Block
68
Off Area Accident Type
Splash Zone Of Riser
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.5
Pipe Smys
42000
Pipe Specification
X-42
Pipe Seam Type
Dsaw
Pipe Manufacturer
National Tube
Pipe Coating Type
Other
Pipe Coating Details
Concrete Coating On Sub-Sea Riser Through Splash Zone
Installation Year
1970
Manufactured Year
1962
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
650
Est Cost Intentional Release
17250
Est Cost Prop Damage
250000
Est Cost Emergency
3000
Est Cost Other
50000
Est Cost Other Details
Blowdown/flare Equipment
Prpty
320900
Accident Psig
726
Mop Psig
999
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
69484
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Tool Will Not Fit In Launcher
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline was operating well below mop/maop.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Atmosphere Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
No
Externally Coated
Yes
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K*** C*******
Preparer Title
Sr. Director
Preparer Email
K************@k**********.com
Preparer Telephone
985-209-2283
Authorizer Name
K*** C*******
Authorizer Title
Sr. Director
Authorizer Telephone
985-209-2283
Authorizer Email
K************@k**********.com
Narrative
On 9/17, fieldwood field supply boat observed a leak on kinetica's wc 68cg platform. Kinetica personnel dispatched and confirmed leak on the 20" riser at the +3' elevation. Kinetica personnel closed block valve on the platform to isolate leak from all production. Kinetica land personnel dispatched to close block valve located onshore to completely isolate pipeline. Kinetica began obtaining necessary blowdown/flare equipment in order to evacuate pressure from line. On 9/23, while equipment was being set up to prepare for evacuation of line, condensate began to mist from the leak location causing a slight silvery sheen. Blowdown/flaring of gas from the line began at noon on 9/23 (675psig). Misting and sheen continued until pressure was reduced to 78psig on the morning of 9/24. Jack-up boat and divers were located and dispatched to wc 68cg platform to evaluate leak. Due to location of leak at the +3' elevation on riser, work had to be performed during periods of calm seas. On 10/10, kinetica contractor completed the repair. On 10/11, pipeline was pressured-up to 300psig. Kinetica personnel discovered repair location was leaking. Block valve on platform was closed to once again isolate production. Pipeline evacuated of pressure. Vessel and contractor located and dispatched to location to initiate repairs. Supplemental report will be prepared and submitted upon completion of repair and placement of pipeline back into service.
| Report Received Date | 2015-10-16 00:00:00 |
|---|---|
| Iyear | 2015 |
| Report Number | 20150125 |
| Supplemental Number | 16937 |
| Report Type | Supplemental Final |
| Operator Id | 38987 PHMSA Enforcement |
| Name | Kinetica Energy Express Llc |
| Operator Street Address | 1001 Mckinney Street, Suite 900 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2015-09-17 17:45:00 |
| Location Latitude | 29.632371 Google Maps OpenStreetMap |
| Location Longitude | -93.038343 Google Maps OpenStreetMap |
| Nrc Rpt Num | 1128765 NRC Report How to search |
| Nrc Rpt Datetime | 2015-09-17 18:30:00 |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 260 |
| Intentional Release | 6900 |
| Accompanying Liquid | 0.1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2015-09-17 18:53:00 |
| Restart Datetime | 2015-11-04 16:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Incident Identified Datetime | 2015-09-17 17:45:00 |
| On Site Datetime | 2015-09-17 18:15:00 |
| On Off Shore | Offshore |
| Off Water Depth | 33 |
| Off Accident Origin | On The Outer Continental Shelf (Ocs) |
| Off Ocs Area | West Cameron |
| Off Ocs Block | 68 |
| Off Area Accident Type | Splash Zone Of Riser |
| Pipe Facility Type | Interstate |
| System Part Involved | Offshore Pipeline, Including Riser And Riser Bend |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 20 |
| Pipe Wall Thickness | 0.5 |
| Pipe Smys | 42000 |
| Pipe Specification | X-42 |
| Pipe Seam Type | Dsaw |
| Pipe Manufacturer | National Tube |
| Pipe Coating Type | Other |
| Pipe Coating Details | Concrete Coating On Sub-Sea Riser Through Splash Zone |
| Installation Year | 1970 |
| Manufactured Year | 1962 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Class Location Type | Class 1 Location |
| Could Be Hca | No |
| Pir Radius | 660 |
| Heat Damage Ind | No |
| Non Heat Damage Ind | No |
| Hca Fatalities Ind | No |
| Est Cost Oper Paid | 0 |
| Est Cost Unintentional Release | 650 |
| Est Cost Intentional Release | 17250 |
| Est Cost Prop Damage | 250000 |
| Est Cost Emergency | 3000 |
| Est Cost Other | 50000 |
| Est Cost Other Details | Blowdown/flare Equipment |
| Prpty | 320900 |
| Accident Psig | 726 |
| Mop Psig | 999 |
| Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Pressure Restriction Ind | No |
| Upstream Valve Type Ind | Manual |
| Downstream Valve Type Ind | Manual |
| Length Segment Isolated | 69484 |
| Internal Inspection Ind | No |
| Tight Mitered Ind | Yes |
| Operation Complications Ind | Yes |
| Other Complications Ind | Yes |
| Inspect Comp Details | Tool Will Not Fit In Launcher |
| Pipeline Function | Transmission System |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Pipeline was operating well below mop/maop. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | External Corrosion |
| Internal External | External Corrosion |
| Visual Exam Results | Localized Pitting |
| Atmosphere Corrosion Ind | Yes |
| Field Exam Basis Ind | Yes |
| Metallurgical Basis Ind | Yes |
| Underground Location | No |
| Externally Coated | Yes |
| Prior Damage | Yes |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | K*** C******* |
| Preparer Title | Sr. Director |
| Preparer Email | K************@k**********.com |
| Preparer Telephone | 985-209-2283 |
| Authorizer Name | K*** C******* |
| Authorizer Title | Sr. Director |
| Authorizer Telephone | 985-209-2283 |
| Authorizer Email | K************@k**********.com |
| Narrative | On 9/17, fieldwood field supply boat observed a leak on kinetica's wc 68cg platform. Kinetica personnel dispatched and confirmed leak on the 20" riser at the +3' elevation. Kinetica personnel closed block valve on the platform to isolate leak from all production. Kinetica land personnel dispatched to close block valve located onshore to completely isolate pipeline. Kinetica began obtaining necessary blowdown/flare equipment in order to evacuate pressure from line. On 9/23, while equipment was being set up to prepare for evacuation of line, condensate began to mist from the leak location causing a slight silvery sheen. Blowdown/flaring of gas from the line began at noon on 9/23 (675psig). Misting and sheen continued until pressure was reduced to 78psig on the morning of 9/24. Jack-up boat and divers were located and dispatched to wc 68cg platform to evaluate leak. Due to location of leak at the +3' elevation on riser, work had to be performed during periods of calm seas. On 10/10, kinetica contractor completed the repair. On 10/11, pipeline was pressured-up to 300psig. Kinetica personnel discovered repair location was leaking. Block valve on platform was closed to once again isolate production. Pipeline evacuated of pressure. Vessel and contractor located and dispatched to location to initiate repairs. Supplemental report will be prepared and submitted upon completion of repair and placement of pipeline back into service. |
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