GTG incident on 2015-09-17 — TX

Operator
Enable Gas Transmission, Llc
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$350,000
Incident datetime
2015-09-17 11:15
Report number
Location
TX
Narrative
On 9/16/15 at 17:33 an enable employee with the el dorado district reports a possible leak was found during a local distribution company leak survey of their pipeline. The enable employee reported the possible leak to system control. Enable's kt-1, the distribution company and 2 foreign pipelines are near the possible leak. The enable employee could not confirm which of the 4 pipelines in the area is leaking. Leak indications were small. On 9/17/15 11:15 enable employees confirmed kt-1 is leaking to system control. At 15:22 local employees calculated and provided system control a cost estimate for repairs of $300,000. On 9/17/15 16:10 system control notified the nrc (report # 1128754) after deciding and determining they would replace the crossing. On 9/19/2015 performed a line stop to eliminate the leaking valve and pipe crossing. The crossing pipe was left in place and a new section of pipe was installed adjacent to the existing pipeline crossing.
Detailed record list
Report Received Date
2015-10-15 00:00:00
Iyear
2015
Report Number
20150124
Supplemental Number
16923
Report Type
Supplemental Final
Operator Id
Name
Enable Gas Transmission, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-09-17 15:22:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-09-17 16:10:00
Commodity Released Type
Natural Gas
Unintentional Release
0.5
Intentional Release
50
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
No, Installed Stoppals
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-09-17 11:15:00
On Site Datetime
2015-09-16 17:13:00
On Off Shore
Onshore
Onshore State Abbreviation
Ar
Onshore Postal Code
71731
Onshore City Name
Not Within A Municipality
Onshore County Name
Union
Designated Location
Survey Station No.
Designated Name
389+10
Pipe Fac Name
Line Kt-1
Segment Name
Route 7 Series 1330
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1953
Material Involved
Material Other Than Carbon Steel Or Plastic
Material Details
Brass
Release Type
Leak
Leak Type
Other
Leak Type Other
Threads And Stem Leaking
Class Location Type
Class 3 Location
Could Be Hca
No
Pir Radius
141
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
2
Est Cost Intentional Release
150
Est Cost Prop Damage
350000
Est Cost Emergency
1000
Est Cost Other
0
Prpty
351152
Accident Psig
315
Mop Psig
420
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
81
Internal Inspection Ind
No
Unsuitable Mainline Ind
Yes
Other Restrictions Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Local Distribution Company
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Small leak that would not have registered on scada system.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Previous Damage Due To Excavation Activity
Ex Party Type
Previous Damage Due To Excavation Activity
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
County Road
Excavator Type
Unknown/other
Excavator Equipment
Unknown/other
Work Performed
Unknown/other
One Call Notified Ind
No
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Previous Damage
Preparer Name
J**** C****
Preparer Title
Dot Compliance Manager
Preparer Email
J**********@e**************.com
Preparer Telephone
3184293664
Authorizer Name
J***** C*****
Authorizer Title
Senior Manager Dot Compliance
Authorizer Telephone
3184293606
Authorizer Email
J************@e**************.com
Narrative
On 9/16/15 at 17:33 an enable employee with the el dorado district reports a possible leak was found during a local distribution company leak survey of their pipeline. The enable employee reported the possible leak to system control. Enable's kt-1, the distribution company and 2 foreign pipelines are near the possible leak. The enable employee could not confirm which of the 4 pipelines in the area is leaking. Leak indications were small. On 9/17/15 11:15 enable employees confirmed kt-1 is leaking to system control. At 15:22 local employees calculated and provided system control a cost estimate for repairs of $300,000. On 9/17/15 16:10 system control notified the nrc (report # 1128754) after deciding and determining they would replace the crossing. On 9/19/2015 performed a line stop to eliminate the leaking valve and pipe crossing. The crossing pipe was left in place and a new section of pipe was installed adjacent to the existing pipeline crossing.
Report Received Date 2015-10-15 00:00:00
Iyear 2015
Report Number 20150124
Supplemental Number 16923
Report Type Supplemental Final
Operator Id 602 PHMSA Enforcement
Name Enable Gas Transmission, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-09-17 15:22:00
Location Latitude 33.15774 Google Maps OpenStreetMap
Location Longitude -92.728778 Google Maps OpenStreetMap
Nrc Rpt Num 1128754 NRC Report How to search
Nrc Rpt Datetime 2015-09-17 16:10:00
Commodity Released Type Natural Gas
Unintentional Release 0.5
Intentional Release 50
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain No, Installed Stoppals
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-09-17 11:15:00
On Site Datetime 2015-09-16 17:13:00
On Off Shore Onshore
Onshore State Abbreviation Ar
Onshore Postal Code 71731
Onshore City Name Not Within A Municipality
Onshore County Name Union
Designated Location Survey Station No.
Designated Name 389+10
Pipe Fac Name Line Kt-1
Segment Name Route 7 Series 1330
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1953
Material Involved Material Other Than Carbon Steel Or Plastic
Material Details Brass
Release Type Leak
Leak Type Other
Leak Type Other Threads And Stem Leaking
Class Location Type Class 3 Location
Could Be Hca No
Pir Radius 141
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 2
Est Cost Intentional Release 150
Est Cost Prop Damage 350000
Est Cost Emergency 1000
Est Cost Other 0
Prpty 351152
Accident Psig 315
Mop Psig 420
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 81
Internal Inspection Ind No
Unsuitable Mainline Ind Yes
Other Restrictions Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Local Distribution Company
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Small leak that would not have registered on scada system.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Previous Damage Due To Excavation Activity
Ex Party Type Previous Damage Due To Excavation Activity
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype County Road
Excavator Type Unknown/other
Excavator Equipment Unknown/other
Work Performed Unknown/other
One Call Notified Ind No
Root Cause Category Miscellaneous Root Causes
Root Cause Type Previous Damage
Preparer Name J**** C****
Preparer Title Dot Compliance Manager
Preparer Email J**********@e**************.com
Preparer Telephone 3184293664
Authorizer Name J***** C*****
Authorizer Title Senior Manager Dot Compliance
Authorizer Telephone 3184293606
Authorizer Email J************@e**************.com
Narrative On 9/16/15 at 17:33 an enable employee with the el dorado district reports a possible leak was found during a local distribution company leak survey of their pipeline. The enable employee reported the possible leak to system control. Enable's kt-1, the distribution company and 2 foreign pipelines are near the possible leak. The enable employee could not confirm which of the 4 pipelines in the area is leaking. Leak indications were small. On 9/17/15 11:15 enable employees confirmed kt-1 is leaking to system control. At 15:22 local employees calculated and provided system control a cost estimate for repairs of $300,000. On 9/17/15 16:10 system control notified the nrc (report # 1128754) after deciding and determining they would replace the crossing. On 9/19/2015 performed a line stop to eliminate the leaking valve and pipe crossing. The crossing pipe was left in place and a new section of pipe was installed adjacent to the existing pipeline crossing.

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