GTG incident on 2015-08-26 — TX

Operator
Gulf South Pipeline Company, Lp
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$625,000
Incident datetime
2015-08-26 20:45
Report number
Location
TX
Narrative
Dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Line disconnected, gas released and ignited at the surface. Cause is still under investigation. 7-7-16 dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Sub-sea connector appeared to be damaged during work activities, thereby, causing a gas release.
Detailed record list
Report Received Date
2015-09-18 00:00:00
Iyear
2015
Report Number
20150114
Supplemental Number
17139
Report Type
Supplemental Final
Operator Id
Name
Gulf South Pipeline Company, Lp
Operator Street Address
9 Greenway Plaza Suite 2800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046
Local Datetime
2015-08-26 20:45:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-08-26 21:40:00
Commodity Released Type
Natural Gas
Unintentional Release
2631
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-26 20:45:00
Restart Datetime
2015-09-06 16:00:00
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-08-26 20:45:00
On Site Datetime
2015-08-26 23:50:00
On Off Shore
Offshore
Off Water Depth
25
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
Eugene Island
Off Ocs Block
95
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Flange Assembly
Installation Year
2006
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
382
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
8098
Est Cost Intentional Release
0
Est Cost Prop Damage
625000
Est Cost Emergency
10000
Est Cost Other
200000
Est Cost Other Details
Investigation
Prpty
843098
Accident Psig
925
Mop Psig
1200
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Length Segment Isolated
174240
Internal Inspection Ind
No
Other Restrictions Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
Sub-Sea Tie-In
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident occurred while contractor was onsite for scheduled outage performed by area.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Num Contractors Tested
24
Num Contractors Failed
0
Cause
Other Incident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
Dive Company Was Jetting To Expose Sub-Sea Tie-In Valve Assembly For Pipeline Abandonment. Sub-Sea Connector Appeared To Be Damaged During Work Activities, Thereby, Causing A Gas Release.
Preparer Name
S****** M********
Preparer Title
Pa Oq And Event Support Program Leader
Preparer Email
S****************@b*****.com
Preparer Telephone
2706886357
Preparer Fax
2706886948
Authorizer Name
J****** B* M******
Authorizer Title
Manager Codes And Standards
Authorizer Telephone
2706886361
Authorizer Email
J***********@b*****.com
Narrative
Dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Line disconnected, gas released and ignited at the surface. Cause is still under investigation. 7-7-16 dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Sub-sea connector appeared to be damaged during work activities, thereby, causing a gas release.
Report Received Date 2015-09-18 00:00:00
Iyear 2015
Report Number 20150114
Supplemental Number 17139
Report Type Supplemental Final
Operator Id 31728 PHMSA Enforcement
Name Gulf South Pipeline Company, Lp
Operator Street Address 9 Greenway Plaza Suite 2800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046
Local Datetime 2015-08-26 20:45:00
Location Latitude 29.043056 Google Maps OpenStreetMap
Location Longitude -91.69944 Google Maps OpenStreetMap
Nrc Rpt Num 1126790 NRC Report How to search
Nrc Rpt Datetime 2015-08-26 21:40:00
Commodity Released Type Natural Gas
Unintentional Release 2631
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-26 20:45:00
Restart Datetime 2015-09-06 16:00:00
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-08-26 20:45:00
On Site Datetime 2015-08-26 23:50:00
On Off Shore Offshore
Off Water Depth 25
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area Eugene Island
Off Ocs Block 95
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Flange Assembly
Installation Year 2006
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 382
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 8098
Est Cost Intentional Release 0
Est Cost Prop Damage 625000
Est Cost Emergency 10000
Est Cost Other 200000
Est Cost Other Details Investigation
Prpty 843098
Accident Psig 925
Mop Psig 1200
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Length Segment Isolated 174240
Internal Inspection Ind No
Other Restrictions Ind Yes
Other Inspection Ind Yes
Internal Inspection Details Sub-Sea Tie-In
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident occurred while contractor was onsite for scheduled outage performed by area.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Num Contractors Tested 24
Num Contractors Failed 0
Cause Other Incident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details Dive Company Was Jetting To Expose Sub-Sea Tie-In Valve Assembly For Pipeline Abandonment. Sub-Sea Connector Appeared To Be Damaged During Work Activities, Thereby, Causing A Gas Release.
Preparer Name S****** M********
Preparer Title Pa Oq And Event Support Program Leader
Preparer Email S****************@b*****.com
Preparer Telephone 2706886357
Preparer Fax 2706886948
Authorizer Name J****** B* M******
Authorizer Title Manager Codes And Standards
Authorizer Telephone 2706886361
Authorizer Email J***********@b*****.com
Narrative Dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Line disconnected, gas released and ignited at the surface. Cause is still under investigation. 7-7-16 dive company was jetting to expose sub-sea tie-in valve assembly for pipeline abandonment. Sub-sea connector appeared to be damaged during work activities, thereby, causing a gas release.

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