GTG incident on 2015-08-12 — TX

Operator
Kinetica Energy Express Llc
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-08-12 14:42
Report number
Location
TX
Narrative
Platform operator for energy xxi contacted kinetica energy express pipeline operations supervisor on 8/12/2015 stating that bubbles had been spotted on the water's surface about 1/2 mile from their platform. Kinetica personnel were dispatched via helicopter to the platform in order to isolate pipeline. At 14:00, platform valves were closed to isolate production from the pipeline. Pressure was monitored to determine if leak was in fact on kinetica's pipeline. At 14:42, it was determined that leak was on kinetica's line. Arrangements were made with producer to relieve pressure from the pipeline to 70 psig so divers could work on pipeline at leak location. Dive vessel was procured and dispatched to the area. Upon arrival in the area, first closed sub-sea tie-in valve in preparation of pipeline repair. Diver excavated leak area and removed concrete coating from pipe. Diver identified a small pinhole leak. The general area had ut inspection performed, and no indications of generalized corrosion were identified. A repair clamp was installed. The platform valves were re-opened. Platform operator was asked to begin production into the line to increase pressure while dive vessel monitored for leaks. After the initial pressurization, the pipeline was returned to service in incremental steps while dive vessel continually monitored location for signs of leak. After determining that the repair was successful, the dive vessel departed location.
Detailed record list
Report Received Date
2015-09-14 00:00:00
Iyear
2015
Report Number
20150112
Supplemental Number
16935
Report Type
Supplemental Final
Operator Id
Name
Kinetica Energy Express Llc
Operator Street Address
1001 Mckinney Street, Suite 900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-12 14:42:00
Location Latitude
Location Longitude
-91.87066667
Nrc Rpt Num
Nrc Rpt Datetime
2015-08-12 15:50:00
Commodity Released Type
Natural Gas
Unintentional Release
30
Intentional Release
623
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-12 14:00:00
Restart Datetime
2015-08-20 16:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-08-12 14:42:00
On Site Datetime
2015-08-12 14:00:00
On Off Shore
Offshore
Off Water Depth
145
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
South Marsh Island
Off Ocs Block
78
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
16
Pipe Wall Thickness
0.375
Pipe Smys
52000
Pipe Specification
5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Nippon
Pipe Coating Type
Epoxy
Installation Year
1991
Manufactured Year
1988
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
83
Est Cost Intentional Release
1713
Est Cost Prop Damage
0
Est Cost Emergency
1600
Est Cost Other
265000
Est Cost Other Details
Cost Of Repair Clamp, Dive Vessel, Divers And Company Personnel
Prpty
268396
Accident Psig
880
Mop Psig
1250
Mop Cfr Section
Mop Cfr Section Details
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
8622
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Subsea Tie-In Configuration Will Not Allow For The Passage Of Inspection Tools
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Platform Operator Identified Bubbles On Sea Surface
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Remote location offshore with pressures well below established maop
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Other
Int Visual Exam Details
Pinhole Identified
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
6:00 Position
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K*** J* C*******
Preparer Title
Senior Director
Preparer Email
K************@k**********.com
Preparer Telephone
9852092283
Preparer Fax
9852236197
Authorizer Name
K*** J* C*******
Authorizer Title
Senior Director
Authorizer Telephone
9852092283
Authorizer Email
K************@k**********.com
Narrative
Platform operator for energy xxi contacted kinetica energy express pipeline operations supervisor on 8/12/2015 stating that bubbles had been spotted on the water's surface about 1/2 mile from their platform. Kinetica personnel were dispatched via helicopter to the platform in order to isolate pipeline. At 14:00, platform valves were closed to isolate production from the pipeline. Pressure was monitored to determine if leak was in fact on kinetica's pipeline. At 14:42, it was determined that leak was on kinetica's line. Arrangements were made with producer to relieve pressure from the pipeline to 70 psig so divers could work on pipeline at leak location. Dive vessel was procured and dispatched to the area. Upon arrival in the area, first closed sub-sea tie-in valve in preparation of pipeline repair. Diver excavated leak area and removed concrete coating from pipe. Diver identified a small pinhole leak. The general area had ut inspection performed, and no indications of generalized corrosion were identified. A repair clamp was installed. The platform valves were re-opened. Platform operator was asked to begin production into the line to increase pressure while dive vessel monitored for leaks. After the initial pressurization, the pipeline was returned to service in incremental steps while dive vessel continually monitored location for signs of leak. After determining that the repair was successful, the dive vessel departed location.
Report Received Date 2015-09-14 00:00:00
Iyear 2015
Report Number 20150112
Supplemental Number 16935
Report Type Supplemental Final
Operator Id 38987 PHMSA Enforcement
Name Kinetica Energy Express Llc
Operator Street Address 1001 Mckinney Street, Suite 900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-12 14:42:00
Location Latitude 28.58 Google Maps OpenStreetMap
Location Longitude -91.87066667 Google Maps OpenStreetMap
Nrc Rpt Num 1125462 NRC Report How to search
Nrc Rpt Datetime 2015-08-12 15:50:00
Commodity Released Type Natural Gas
Unintentional Release 30
Intentional Release 623
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-12 14:00:00
Restart Datetime 2015-08-20 16:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-08-12 14:42:00
On Site Datetime 2015-08-12 14:00:00
On Off Shore Offshore
Off Water Depth 145
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area South Marsh Island
Off Ocs Block 78
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 16
Pipe Wall Thickness 0.375
Pipe Smys 52000
Pipe Specification 5l
Pipe Seam Type Seamless
Pipe Manufacturer Nippon
Pipe Coating Type Epoxy
Installation Year 1991
Manufactured Year 1988
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 83
Est Cost Intentional Release 1713
Est Cost Prop Damage 0
Est Cost Emergency 1600
Est Cost Other 265000
Est Cost Other Details Cost Of Repair Clamp, Dive Vessel, Divers And Company Personnel
Prpty 268396
Accident Psig 880
Mop Psig 1250
Mop Cfr Section Other View CFR 49 §192
Mop Cfr Section Details Not On Omb-Approved Form When Submitted
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 8622
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Subsea Tie-In Configuration Will Not Allow For The Passage Of Inspection Tools
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Platform Operator Identified Bubbles On Sea Surface
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Remote location offshore with pressures well below established maop
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Other
Int Visual Exam Details Pinhole Identified
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details 6:00 Position
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K*** J* C*******
Preparer Title Senior Director
Preparer Email K************@k**********.com
Preparer Telephone 9852092283
Preparer Fax 9852236197
Authorizer Name K*** J* C*******
Authorizer Title Senior Director
Authorizer Telephone 9852092283
Authorizer Email K************@k**********.com
Narrative Platform operator for energy xxi contacted kinetica energy express pipeline operations supervisor on 8/12/2015 stating that bubbles had been spotted on the water's surface about 1/2 mile from their platform. Kinetica personnel were dispatched via helicopter to the platform in order to isolate pipeline. At 14:00, platform valves were closed to isolate production from the pipeline. Pressure was monitored to determine if leak was in fact on kinetica's pipeline. At 14:42, it was determined that leak was on kinetica's line. Arrangements were made with producer to relieve pressure from the pipeline to 70 psig so divers could work on pipeline at leak location. Dive vessel was procured and dispatched to the area. Upon arrival in the area, first closed sub-sea tie-in valve in preparation of pipeline repair. Diver excavated leak area and removed concrete coating from pipe. Diver identified a small pinhole leak. The general area had ut inspection performed, and no indications of generalized corrosion were identified. A repair clamp was installed. The platform valves were re-opened. Platform operator was asked to begin production into the line to increase pressure while dive vessel monitored for leaks. After the initial pressurization, the pipeline was returned to service in incremental steps while dive vessel continually monitored location for signs of leak. After determining that the repair was successful, the dive vessel departed location.

All rights reserved. Copyright © by ClearPHMSA