GTG incident on 2015-07-18 — TX

Operator
Colorado Interstate Gas Co
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2015-07-18 17:24
Report number
Location
TX
Narrative
A solenoid valve on the tower switch valve failed, rendering the air dryer inoperable. This allowed water to enter the esd system causing the esd vent valve to activate (the water interfered with the esd's pneumatic operation). Gas was released through a 6" vent stack into the atmosphere. A volume greater than the reporting threshold of 3,000 mcf was released resulting in the incident report to the nrc. The instrument air dryer has been repaired and the facility was successfully placed back into service.
Detailed record list
Report Received Date
2015-08-12 00:00:00
Iyear
2015
Report Number
20150102
Supplemental Number
16834
Report Type
Original Final
Operator Id
Name
Colorado Interstate Gas Co
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-07-18 17:22:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-07-18 19:07:00
Commodity Released Type
Natural Gas
Unintentional Release
3600
Intentional Release
500
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-18 17:46:00
Restart Datetime
2015-07-22 14:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-07-18 17:24:00
On Site Datetime
2015-07-18 17:46:00
On Off Shore
Onshore
Onshore State Abbreviation
Co
Onshore Postal Code
80103
Onshore City Name
Byers
Onshore County Name
Arapahoe
Designated Location
Milepost
Designated Name
1.0
Pipe Fac Name
Latigo Storage
Segment Name
Yard Piping
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Belowground Storage, Including Associated Equipment And Piping
Item Involved
Other
Item Involved Details
Esd Vent Valve
Installation Year
1978
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Release Through 6" Vent Valve Outlet Pipe.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
207
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
9900
Est Cost Intentional Release
1375
Est Cost Prop Damage
2500
Est Cost Emergency
1500
Est Cost Other
0
Prpty
15275
Accident Psig
1520
Mop Psig
2130
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission In Storage Field
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room was not involved in any way.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Eq Failure Details
Instrument Air Dryer Failed Allowing Water To Get Into The Esd System
Eq Additional Other Ind
Yes
Eq Additional Other Details
Solenoid Valve On Tower Switch Valve Failed.
Preparer Name
K****** C P*****
Preparer Title
Sr. Engineer
Preparer Email
K*********@k***********.com
Preparer Telephone
2053257554
Preparer Fax
2053253508
Authorizer Name
R*** G*****
Authorizer Title
Director Codes Standards
Authorizer Telephone
7134205433
Authorizer Email
R**********@k***********.com
Narrative
A solenoid valve on the tower switch valve failed, rendering the air dryer inoperable. This allowed water to enter the esd system causing the esd vent valve to activate (the water interfered with the esd's pneumatic operation). Gas was released through a 6" vent stack into the atmosphere. A volume greater than the reporting threshold of 3,000 mcf was released resulting in the incident report to the nrc. The instrument air dryer has been repaired and the facility was successfully placed back into service.
Report Received Date 2015-08-12 00:00:00
Iyear 2015
Report Number 20150102
Supplemental Number 16834
Report Type Original Final
Operator Id 2564 PHMSA Enforcement
Name Colorado Interstate Gas Co
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-07-18 17:22:00
Location Latitude 39.6085 Google Maps OpenStreetMap
Location Longitude -104.35013 Google Maps OpenStreetMap
Nrc Rpt Num 1123182 NRC Report How to search
Nrc Rpt Datetime 2015-07-18 19:07:00
Commodity Released Type Natural Gas
Unintentional Release 3600
Intentional Release 500
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-18 17:46:00
Restart Datetime 2015-07-22 14:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-07-18 17:24:00
On Site Datetime 2015-07-18 17:46:00
On Off Shore Onshore
Onshore State Abbreviation Co
Onshore Postal Code 80103
Onshore City Name Byers
Onshore County Name Arapahoe
Designated Location Milepost
Designated Name 1.0
Pipe Fac Name Latigo Storage
Segment Name Yard Piping
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Belowground Storage, Including Associated Equipment And Piping
Item Involved Other
Item Involved Details Esd Vent Valve
Installation Year 1978
Material Involved Carbon Steel
Release Type Other
Release Type Details Release Through 6" Vent Valve Outlet Pipe.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 207
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 9900
Est Cost Intentional Release 1375
Est Cost Prop Damage 2500
Est Cost Emergency 1500
Est Cost Other 0
Prpty 15275
Accident Psig 1520
Mop Psig 2130
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission In Storage Field
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room was not involved in any way.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Eq Failure Details Instrument Air Dryer Failed Allowing Water To Get Into The Esd System
Eq Additional Other Ind Yes
Eq Additional Other Details Solenoid Valve On Tower Switch Valve Failed.
Preparer Name K****** C P*****
Preparer Title Sr. Engineer
Preparer Email K*********@k***********.com
Preparer Telephone 2053257554
Preparer Fax 2053253508
Authorizer Name R*** G*****
Authorizer Title Director Codes Standards
Authorizer Telephone 7134205433
Authorizer Email R**********@k***********.com
Narrative A solenoid valve on the tower switch valve failed, rendering the air dryer inoperable. This allowed water to enter the esd system causing the esd vent valve to activate (the water interfered with the esd's pneumatic operation). Gas was released through a 6" vent stack into the atmosphere. A volume greater than the reporting threshold of 3,000 mcf was released resulting in the incident report to the nrc. The instrument air dryer has been repaired and the facility was successfully placed back into service.

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