GD incident on 2015-07-06 — MO

Operator
Missouri Gas Energy
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,301
Incident datetime
2015-07-06 07:54
Report number
Location
MO, CLAY
Narrative
A contractor operating a grader failed to observe facility location marks and punctured an approximately 22 square inch hole in a 12 inch steel main. It is our understanding the contractor was under the impression the 12 inch steel main was relocated as a result of a recent main relocation project. The construction plans did not indicate the 12 inch steel main was to be relocated. Emergency responders were on-site and assisted in traffic control. Gas was made safe by closing a 6 inch valve on church road, north of the damage, stoppling a 6 inch three-way tee, northeast of damage at pleasant valley road and liberty parkway, closing the outlet valve of regulator station #007, south of damage at highway 69 and squeezing off a 6 inch plastic main on pleasant valley road, west of church road. A 30 inch long full circumferential band and a 48 inch long sleeve were welded over the damaged section of pipe. Repairs were completed at 16:27 on july 6, 2016, and service tech began relighting 210 customers who lost service.
Detailed record list
Occurred At
2015-07-06 07:54:00
Year
2015
Report Received Date
2015-08-05 00:00:00
Iyear
2015.0
Report Number
20150078.0
Supplemental Number
16294.0
Report Type
Supplemental Final
Operator Id
Name
Missouri Gas Energy
Operator Street Address
3420 Broadway
Operator City Name
Kansas City
Operator State Abbreviation
MO
Operator Postal Code
64111
Local Datetime
2015-07-06 07:35:00
Location Street Address
Pleasant Valley Street & I-35
Location City Name
Pleasant Valley
Location County Name
Clay
Location State Abbreviation
MO
Location Postal Code
64068
Location Latitude
Location Longitude
Nrc Rpt Datetime
2015-07-06 10:45:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4471.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2015-07-06 07:54:00
On Site Datetime
2015-07-06 08:10:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1959.0
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
11.0
Puncture Circum
4.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
26301.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Est Cost Unintentional Release
23483.0
Prpty
50284.0
Commercial Affected
20.0
Industrial Affected
0.0
Residences Affected
190.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
33.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Notification from the third party of direct cause of mechanical punture from grader.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
Interstate Highway
Excavator Type
Contractor
Excavator Equipment
Grader/scraper
Work Performed
Grading
One Call Notified Ind
Yes
One Call Ticket Num
151820607
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
9.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
P****** S*******
Preparer Title
Manager Of Pipeline Safety And Compliance
Preparer Email
P***************@t**************.com
Preparer Telephone
(314) 349-2936
Authorizer Name
C**** R* H********
Authorizer Title
Vice President Of Operations Services
Authorizer Telephone
(314) 349-2972
Authorizer Email
C**************@t**************.com
Narrative
A contractor operating a grader failed to observe facility location marks and punctured an approximately 22 square inch hole in a 12 inch steel main. It is our understanding the contractor was under the impression the 12 inch steel main was relocated as a result of a recent main relocation project. The construction plans did not indicate the 12 inch steel main was to be relocated. Emergency responders were on-site and assisted in traffic control. Gas was made safe by closing a 6 inch valve on church road, north of the damage, stoppling a 6 inch three-way tee, northeast of damage at pleasant valley road and liberty parkway, closing the outlet valve of regulator station #007, south of damage at highway 69 and squeezing off a 6 inch plastic main on pleasant valley road, west of church road. A 30 inch long full circumferential band and a 48 inch long sleeve were welded over the damaged section of pipe. Repairs were completed at 16:27 on july 6, 2016, and service tech began relighting 210 customers who lost service.
Occurred At 2015-07-06 07:54:00
Year 2015
Report Received Date 2015-08-05 00:00:00
Iyear 2015.0
Report Number 20150078.0
Supplemental Number 16294.0
Report Type Supplemental Final
Operator Id 30769 PHMSA Enforcement
Name Missouri Gas Energy
Operator Street Address 3420 Broadway
Operator City Name Kansas City
Operator State Abbreviation MO
Operator Postal Code 64111
Local Datetime 2015-07-06 07:35:00
Location Street Address Pleasant Valley Street & I-35
Location City Name Pleasant Valley
Location County Name Clay
Location State Abbreviation MO
Location Postal Code 64068
Location Latitude 39.213154 Google Maps OpenStreetMap
Location Longitude -94.479094 Google Maps OpenStreetMap
Nrc Rpt Datetime 2015-07-06 10:45:00
Nrc Rpt Num 1121959 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4471.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2015-07-06 07:54:00
On Site Datetime 2015-07-06 08:10:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1959.0
Pipe Diameter 12.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Mechanical Puncture
Puncture Axial 11.0
Puncture Circum 4.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 26301.0
Est Cost Emergency 500.0
Est Cost Other 0.0
Est Cost Unintentional Release 23483.0
Prpty 50284.0
Commercial Affected 20.0
Industrial Affected 0.0
Residences Affected 190.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 33.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Notification from the third party of direct cause of mechanical punture from grader.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype Interstate Highway
Excavator Type Contractor
Excavator Equipment Grader/scraper
Work Performed Grading
One Call Notified Ind Yes
One Call Ticket Num 151820607
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 9.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name P****** S*******
Preparer Title Manager Of Pipeline Safety And Compliance
Preparer Email P***************@t**************.com
Preparer Telephone (314) 349-2936
Authorizer Name C**** R* H********
Authorizer Title Vice President Of Operations Services
Authorizer Telephone (314) 349-2972
Authorizer Email C**************@t**************.com
Narrative A contractor operating a grader failed to observe facility location marks and punctured an approximately 22 square inch hole in a 12 inch steel main. It is our understanding the contractor was under the impression the 12 inch steel main was relocated as a result of a recent main relocation project. The construction plans did not indicate the 12 inch steel main was to be relocated. Emergency responders were on-site and assisted in traffic control. Gas was made safe by closing a 6 inch valve on church road, north of the damage, stoppling a 6 inch three-way tee, northeast of damage at pleasant valley road and liberty parkway, closing the outlet valve of regulator station #007, south of damage at highway 69 and squeezing off a 6 inch plastic main on pleasant valley road, west of church road. A 30 inch long full circumferential band and a 48 inch long sleeve were welded over the damaged section of pipe. Repairs were completed at 16:27 on july 6, 2016, and service tech began relighting 210 customers who lost service.

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