GD incident on 2015-06-14 — NY

Operator
Keyspan Energy Delivery - Ny City
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000,000
Incident datetime
2015-06-14 21:00
Report number
Location
NY, KINGS
Narrative
A 60" steel water main, operating in the range of 90 to 105 psi, ruptured in close proximity (6" below) to national grid 12" steel lp main . Jetting caused by the water pressure bore a 2.5" hole into 12" steel lp main. The rapid escape of the water flooded the gas main, resulting in a 1-mile pipeline outage, along with 98 service outages affecting 1367 customers. National grid received multiple service calls from customers starting at 3 pm on 6/14/2015, responded to those calls, and by 9 pm determined the cause of the multiple outages.
Detailed record list
Occurred At
2015-06-14 21:00:00
Year
2015
Report Received Date
2015-07-14 00:00:00
Iyear
2015.0
Report Number
20150069.0
Supplemental Number
16116.0
Report Type
Original Final
Operator Id
Name
Keyspan Energy Delivery - Ny City
Operator Street Address
2 Hanson Place
Operator City Name
Brooklyn
Operator State Abbreviation
NY
Operator Postal Code
11217
Local Datetime
2015-06-14 00:00:00
Location Street Address
Kings Highway And East 98th Street
Location City Name
Brooklyn
Location County Name
Kings
Location State Abbreviation
NY
Location Postal Code
11212
Location Latitude
Location Longitude
Nrc Rpt Datetime
2015-06-16 11:00:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
0.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2015-06-14 21:00:00
On Site Datetime
2015-06-14 21:00:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1972.0
Pipe Diameter
12.75
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Steel Seam Type Details
Seamless
Wt Steel
0.375
Release Type
Mechanical Puncture
Puncture Axial
2.5
Puncture Circum
2.5
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
1000000.0
Est Cost Emergency
28500.0
Est Cost Other
0.0
Est Cost Unintentional Release
10.0
Prpty
1028510.0
Commercial Affected
60.0
Industrial Affected
10.0
Residences Affected
1297.0
Accident Psig
0.0
Normal Psig
0.25
Mop Psig
0.64
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No abnormal conditions detected in the surrounding area. The incident was detected as a result of customer calls of no gas within the 1-mile boundary of flooding.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
60" Steel Water Main, Operating In The Range Of 90 To 105 Psi, Ruptured In Close Proximity To National Grid 12" Steel Lp Main . Jetting Caused By The Water Pressure Bore A 2.5" Hole Into 12" Steel Lp Main.
Preparer Name
C****** B*****
Preparer Title
Prin Prog Mgr Operations Codes And Policy
Preparer Email
C*************@n***********.com
Preparer Telephone
5164924469
Authorizer Name
C****** B*****
Authorizer Title
Prin Prog Mgr- Operations Codes And Policy
Authorizer Telephone
5164924469
Authorizer Email
C*************@g****.com
Narrative
A 60" steel water main, operating in the range of 90 to 105 psi, ruptured in close proximity (6" below) to national grid 12" steel lp main . Jetting caused by the water pressure bore a 2.5" hole into 12" steel lp main. The rapid escape of the water flooded the gas main, resulting in a 1-mile pipeline outage, along with 98 service outages affecting 1367 customers. National grid received multiple service calls from customers starting at 3 pm on 6/14/2015, responded to those calls, and by 9 pm determined the cause of the multiple outages.
Occurred At 2015-06-14 21:00:00
Year 2015
Report Received Date 2015-07-14 00:00:00
Iyear 2015.0
Report Number 20150069.0
Supplemental Number 16116.0
Report Type Original Final
Operator Id 1800 PHMSA Enforcement
Name Keyspan Energy Delivery - Ny City
Operator Street Address 2 Hanson Place
Operator City Name Brooklyn
Operator State Abbreviation NY
Operator Postal Code 11217
Local Datetime 2015-06-14 00:00:00
Location Street Address Kings Highway And East 98th Street
Location City Name Brooklyn
Location County Name Kings
Location State Abbreviation NY
Location Postal Code 11212
Location Latitude 40.662012 Google Maps OpenStreetMap
Location Longitude -73.919579 Google Maps OpenStreetMap
Nrc Rpt Datetime 2015-06-16 11:00:00
Nrc Rpt Num 1119934 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 0.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2015-06-14 21:00:00
On Site Datetime 2015-06-14 21:00:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1972.0
Pipe Diameter 12.75
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Steel Seam Type Details Seamless
Wt Steel 0.375
Release Type Mechanical Puncture
Puncture Axial 2.5
Puncture Circum 2.5
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 1000000.0
Est Cost Emergency 28500.0
Est Cost Other 0.0
Est Cost Unintentional Release 10.0
Prpty 1028510.0
Commercial Affected 60.0
Industrial Affected 10.0
Residences Affected 1297.0
Accident Psig 0.0
Normal Psig 0.25
Mop Psig 0.64
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No abnormal conditions detected in the surrounding area. The incident was detected as a result of customer calls of no gas within the 1-mile boundary of flooding.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details 60" Steel Water Main, Operating In The Range Of 90 To 105 Psi, Ruptured In Close Proximity To National Grid 12" Steel Lp Main . Jetting Caused By The Water Pressure Bore A 2.5" Hole Into 12" Steel Lp Main.
Preparer Name C****** B*****
Preparer Title Prin Prog Mgr Operations Codes And Policy
Preparer Email C*************@n***********.com
Preparer Telephone 5164924469
Authorizer Name C****** B*****
Authorizer Title Prin Prog Mgr- Operations Codes And Policy
Authorizer Telephone 5164924469
Authorizer Email C*************@g****.com
Narrative A 60" steel water main, operating in the range of 90 to 105 psi, ruptured in close proximity (6" below) to national grid 12" steel lp main . Jetting caused by the water pressure bore a 2.5" hole into 12" steel lp main. The rapid escape of the water flooded the gas main, resulting in a 1-mile pipeline outage, along with 98 service outages affecting 1367 customers. National grid received multiple service calls from customers starting at 3 pm on 6/14/2015, responded to those calls, and by 9 pm determined the cause of the multiple outages.

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