GTG incident on 2015-03-28 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$45,000
Incident datetime
2015-03-28 07:20
Report number
Location
TX
Narrative
On 3/28/2015 at 07:20 am, gas control received a call from a third party reporting a possible leak at the decordova compressor station and an enterprise technician was dispatched to the decordova compressor station. Upon the technicians arrival at approximately 08:10 am, the technician discovered that the unit suction valve on unit 810 did not completely close (90% closure) at time gas control remotely shut down compressor (scheduled shutdown). The technician manually shut the valve, thus ending the unintentional gas through the blow down stack. The valve was tested several times and found to be faulty with worn valve seats and a bad actuator. Unit 810 has been taken out of service until further notice (locked out-tagged out). A new valve and actuator have been ordered for replacement/repair. On 4/23/2015, new valve and actuator installation has been completed.
Detailed record list
Report Received Date
2015-04-17 00:00:00
Iyear
2015
Report Number
20150053
Supplemental Number
16740
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-03-28 11:20:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-03-28 11:30:00
Commodity Released Type
Natural Gas
Unintentional Release
7450
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-03-28 08:10:00
Still Shutdown Ind
Yes
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-03-28 07:20:00
On Site Datetime
2015-03-28 08:10:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
76048
Onshore City Name
Grandbury
Onshore County Name
Hood
Designated Location
Milepost
Designated Name
Decordova
Pipe Fac Name
North Texas Gas System
Segment Name
Line 225
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
805
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
18625
Est Cost Intentional Release
0
Est Cost Prop Damage
45000
Est Cost Emergency
500
Est Cost Other
0
Prpty
64125
Accident Psig
925
Mop Psig
1041
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary. Leak was detectable but did not meet alarm thresholds or reporting criteria by the controller in the control room; therefor, controller was not the cause nor a contributing factor to the incident. No other factors were determined requiring an investigation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Compressor Unit 812 Suction Valve
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Seats And Actuator Failure
Preparer Name
M****** D* S****
Preparer Title
Compliance Speciliest
Preparer Email
M******@e****.com
Preparer Telephone
713-381-5650
Authorizer Name
M****** D* S****
Authorizer Title
Compliance Speciliest
Authorizer Telephone
713-381-5650
Authorizer Email
M******@e****.com
Narrative
On 3/28/2015 at 07:20 am, gas control received a call from a third party reporting a possible leak at the decordova compressor station and an enterprise technician was dispatched to the decordova compressor station. Upon the technicians arrival at approximately 08:10 am, the technician discovered that the unit suction valve on unit 810 did not completely close (90% closure) at time gas control remotely shut down compressor (scheduled shutdown). The technician manually shut the valve, thus ending the unintentional gas through the blow down stack. The valve was tested several times and found to be faulty with worn valve seats and a bad actuator. Unit 810 has been taken out of service until further notice (locked out-tagged out). A new valve and actuator have been ordered for replacement/repair. On 4/23/2015, new valve and actuator installation has been completed.
Report Received Date 2015-04-17 00:00:00
Iyear 2015
Report Number 20150053
Supplemental Number 16740
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-03-28 11:20:00
Location Latitude 32.19562 Google Maps OpenStreetMap
Location Longitude -97.444019 Google Maps OpenStreetMap
Nrc Rpt Num 1111962 NRC Report How to search
Nrc Rpt Datetime 2015-03-28 11:30:00
Commodity Released Type Natural Gas
Unintentional Release 7450
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-03-28 08:10:00
Still Shutdown Ind Yes
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-03-28 07:20:00
On Site Datetime 2015-03-28 08:10:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 76048
Onshore City Name Grandbury
Onshore County Name Hood
Designated Location Milepost
Designated Name Decordova
Pipe Fac Name North Texas Gas System
Segment Name Line 225
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 805
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 18625
Est Cost Intentional Release 0
Est Cost Prop Damage 45000
Est Cost Emergency 500
Est Cost Other 0
Prpty 64125
Accident Psig 925
Mop Psig 1041
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary. Leak was detectable but did not meet alarm thresholds or reporting criteria by the controller in the control room; therefor, controller was not the cause nor a contributing factor to the incident. No other factors were determined requiring an investigation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Compressor Unit 812 Suction Valve
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Seats And Actuator Failure
Preparer Name M****** D* S****
Preparer Title Compliance Speciliest
Preparer Email M******@e****.com
Preparer Telephone 713-381-5650
Authorizer Name M****** D* S****
Authorizer Title Compliance Speciliest
Authorizer Telephone 713-381-5650
Authorizer Email M******@e****.com
Narrative On 3/28/2015 at 07:20 am, gas control received a call from a third party reporting a possible leak at the decordova compressor station and an enterprise technician was dispatched to the decordova compressor station. Upon the technicians arrival at approximately 08:10 am, the technician discovered that the unit suction valve on unit 810 did not completely close (90% closure) at time gas control remotely shut down compressor (scheduled shutdown). The technician manually shut the valve, thus ending the unintentional gas through the blow down stack. The valve was tested several times and found to be faulty with worn valve seats and a bad actuator. Unit 810 has been taken out of service until further notice (locked out-tagged out). A new valve and actuator have been ordered for replacement/repair. On 4/23/2015, new valve and actuator installation has been completed.

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