GTG incident on 2015-03-09 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$225
Incident datetime
2015-03-09 06:00
Report number
Location
TX
Narrative
At 06:00 operations technician arrived at the real compressor station and discovered a relief valve venting natural gas to atmosphere on the c-200 compressor unit. Technician responded immediately and closed the isolation valve to the 3x4" relief valve thus, ending the event. This unit has two relief valves on the unit operating in parallel as a redundant system. Upon further investigation, it was determined that the relief valve lifted prematurely due to a leak on the sensing line for the relief valve due to excessive vibration. The sensing line tubing was replaced with additional supports to prevent future recurrence.
Detailed record list
Report Received Date
2015-04-02 00:00:00
Iyear
2015
Report Number
20150047
Supplemental Number
16710
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-03-09 05:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-03-09 07:40:00
Commodity Released Type
Natural Gas
Unintentional Release
6600
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Compressor Unit Was Not Shut Down Due To Having Redundant Relief Valves
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-03-09 06:00:00
On Site Datetime
2015-03-09 06:00:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
78873
Onshore City Name
Leaky
Onshore County Name
Real
Designated Location
Milepost
Designated Name
Real Station
Pipe Fac Name
G************************@ ***********************
Segment Name
Line 146-Grey Ranch-New Braunfels
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2006
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Relief Valve Relieved Prematurely Due To Leak In Sensing Line Caused By Excessive Vibration
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
644
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
16480
Est Cost Intentional Release
0
Est Cost Prop Damage
225
Est Cost Emergency
0
Est Cost Other
0
Prpty
16705
Accident Psig
765
Mop Psig
858
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary. Since the controller or control room did not cause nor contribute to the incident. No pressure alarm thresholds were met; no alarms were activated. No other factors were determined requiring an investigation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Relief Valve Relieved Prematurely Due To Leak In Sensing Line.
Preparer Name
M****** D* S****
Preparer Title
Compliance Specialist
Preparer Email
M******@e****.com
Preparer Telephone
713-381-5650
Authorizer Name
M****** D* S****
Authorizer Title
Compliance Specialist
Authorizer Telephone
713-381-5650
Authorizer Email
M******@e****.com
Narrative
At 06:00 operations technician arrived at the real compressor station and discovered a relief valve venting natural gas to atmosphere on the c-200 compressor unit. Technician responded immediately and closed the isolation valve to the 3x4" relief valve thus, ending the event. This unit has two relief valves on the unit operating in parallel as a redundant system. Upon further investigation, it was determined that the relief valve lifted prematurely due to a leak on the sensing line for the relief valve due to excessive vibration. The sensing line tubing was replaced with additional supports to prevent future recurrence.
Report Received Date 2015-04-02 00:00:00
Iyear 2015
Report Number 20150047
Supplemental Number 16710
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-03-09 05:00:00
Location Latitude 30.014769 Google Maps OpenStreetMap
Location Longitude -99.500719 Google Maps OpenStreetMap
Nrc Rpt Num 1109995 NRC Report How to search
Nrc Rpt Datetime 2015-03-09 07:40:00
Commodity Released Type Natural Gas
Unintentional Release 6600
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Compressor Unit Was Not Shut Down Due To Having Redundant Relief Valves
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-03-09 06:00:00
On Site Datetime 2015-03-09 06:00:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 78873
Onshore City Name Leaky
Onshore County Name Real
Designated Location Milepost
Designated Name Real Station
Pipe Fac Name G************************@ ***********************
Segment Name Line 146-Grey Ranch-New Braunfels
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Valve
Valve Type Relief Valve
Installation Year 2006
Material Involved Carbon Steel
Release Type Other
Release Type Details Relief Valve Relieved Prematurely Due To Leak In Sensing Line Caused By Excessive Vibration
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 644
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 16480
Est Cost Intentional Release 0
Est Cost Prop Damage 225
Est Cost Emergency 0
Est Cost Other 0
Prpty 16705
Accident Psig 765
Mop Psig 858
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary. Since the controller or control room did not cause nor contribute to the incident. No pressure alarm thresholds were met; no alarms were activated. No other factors were determined requiring an investigation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Relief Valve Relieved Prematurely Due To Leak In Sensing Line.
Preparer Name M****** D* S****
Preparer Title Compliance Specialist
Preparer Email M******@e****.com
Preparer Telephone 713-381-5650
Authorizer Name M****** D* S****
Authorizer Title Compliance Specialist
Authorizer Telephone 713-381-5650
Authorizer Email M******@e****.com
Narrative At 06:00 operations technician arrived at the real compressor station and discovered a relief valve venting natural gas to atmosphere on the c-200 compressor unit. Technician responded immediately and closed the isolation valve to the 3x4" relief valve thus, ending the event. This unit has two relief valves on the unit operating in parallel as a redundant system. Upon further investigation, it was determined that the relief valve lifted prematurely due to a leak on the sensing line for the relief valve due to excessive vibration. The sensing line tubing was replaced with additional supports to prevent future recurrence.

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