GD incident on 2015-02-27 — CA

Operator
Pacific Gas & Electric Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$163,600
Incident datetime
2015-02-27 13:51
Report number
Location
CA, SACRAMENTO
Narrative
At 1351 hours on february 27, 2015, pg&e was notified of a third-party dig-in near the intersection of elk grove-florin road and gerber road in sacramento. The third-party (western engineering) was using a backhoe to dig new underground services (sewer manholes) when they struck an 8-inch plastic distribution main, causing an unintentional release of natural gas. Western engineering provided a valid USA ticket (#413394). Pg&e facilities were properly located and marked, but the excavator failed to hand dig, expose, and protect the facilities before using mechanical equipment. Pg&e was onsite at 1405 hours. Gas was shut in by 1737 hours by excavating and squeezing the distribution main. Fire department, police, and sacramento media (channel 10 and 3) were observed on scene. Traffic was blocked on gerber road (east of elk grove-florin road) and rerouted from the area. The incident was reported to the cpuc and DOT due to damages likely exceeding $50,000. There were no injuries or fatalities reported. Additionally, there was no ignition and the estimated volume of gas released was less than three million cubic feet. Approximately 768 residential customers lost gas service during the incident. Pg&e restored gas service to all the available customers (I.E. Approximately 431 customers) by 0200 hours on february 28, 2015. By march 1, 2015, pg&e restored gas service for approximately 323 additional customers. As of march 26, 2015, service was restored for an additional eight customers; the remaining six homes are vacant.
Detailed record list
Occurred At
2015-02-27 13:51:00
Year
2015
Report Received Date
2015-03-26 00:00:00
Iyear
2015.0
Report Number
20150032.0
Supplemental Number
16050.0
Report Type
Supplemental Final
Operator Id
Name
Pacific Gas & Electric Co
Operator Street Address
6121 Bollinger Canyon Rd.
Operator City Name
San Ramon
Operator State Abbreviation
CA
Operator Postal Code
94583
Local Datetime
2015-02-27 13:51:00
Location Street Address
Elk-Grove Florin Rd And Gerber Rd
Location City Name
Sacramento
Location County Name
Sacramento
Location State Abbreviation
CA
Location Postal Code
95829
Location Latitude
Location Longitude
-121.3673103
Nrc Rpt Datetime
2015-02-27 16:10:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
293.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2015-02-27 13:51:00
On Site Datetime
2015-02-27 14:05:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2008.0
Pipe Diameter
8.0
Pipe Specification
Astm D2513
Pipe Manufacturer
Driscoplex
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
13.5
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
163600.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
1260.0
Prpty
164860.0
Commercial Affected
768.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
54.0
Normal Psig
57.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Business
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
Yes
One Call Ticket Num
413394
One Call Center Name
Usa North 811
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
8.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
C****** C****
Preparer Title
Gas Engineer
Preparer Email
C***@p**.com
Preparer Telephone
9253285727
Authorizer Name
L**** D*******
Authorizer Title
Manager
Authorizer Telephone
9253285756
Authorizer Email
L***@p**.com
Narrative
At 1351 hours on february 27, 2015, pg&e was notified of a third-party dig-in near the intersection of elk grove-florin road and gerber road in sacramento. The third-party (western engineering) was using a backhoe to dig new underground services (sewer manholes) when they struck an 8-inch plastic distribution main, causing an unintentional release of natural gas. Western engineering provided a valid USA ticket (#413394). Pg&e facilities were properly located and marked, but the excavator failed to hand dig, expose, and protect the facilities before using mechanical equipment. Pg&e was onsite at 1405 hours. Gas was shut in by 1737 hours by excavating and squeezing the distribution main. Fire department, police, and sacramento media (channel 10 and 3) were observed on scene. Traffic was blocked on gerber road (east of elk grove-florin road) and rerouted from the area. The incident was reported to the cpuc and DOT due to damages likely exceeding $50,000. There were no injuries or fatalities reported. Additionally, there was no ignition and the estimated volume of gas released was less than three million cubic feet. Approximately 768 residential customers lost gas service during the incident. Pg&e restored gas service to all the available customers (I.E. Approximately 431 customers) by 0200 hours on february 28, 2015. By march 1, 2015, pg&e restored gas service for approximately 323 additional customers. As of march 26, 2015, service was restored for an additional eight customers; the remaining six homes are vacant.
Occurred At 2015-02-27 13:51:00
Year 2015
Report Received Date 2015-03-26 00:00:00
Iyear 2015.0
Report Number 20150032.0
Supplemental Number 16050.0
Report Type Supplemental Final
Operator Id 15007 PHMSA Enforcement
Name Pacific Gas & Electric Co
Operator Street Address 6121 Bollinger Canyon Rd.
Operator City Name San Ramon
Operator State Abbreviation CA
Operator Postal Code 94583
Local Datetime 2015-02-27 13:51:00
Location Street Address Elk-Grove Florin Rd And Gerber Rd
Location City Name Sacramento
Location County Name Sacramento
Location State Abbreviation CA
Location Postal Code 95829
Location Latitude 38.48179267 Google Maps OpenStreetMap
Location Longitude -121.3673103 Google Maps OpenStreetMap
Nrc Rpt Datetime 2015-02-27 16:10:00
Nrc Rpt Num 1109272 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 293.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2015-02-27 13:51:00
On Site Datetime 2015-02-27 14:05:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2008.0
Pipe Diameter 8.0
Pipe Specification Astm D2513
Pipe Manufacturer Driscoplex
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 13.5
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 163600.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 1260.0
Prpty 164860.0
Commercial Affected 768.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 54.0
Normal Psig 57.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Business
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind Yes
One Call Ticket Num 413394
One Call Center Name Usa North 811
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 8.0
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name C****** C****
Preparer Title Gas Engineer
Preparer Email C***@p**.com
Preparer Telephone 9253285727
Authorizer Name L**** D*******
Authorizer Title Manager
Authorizer Telephone 9253285756
Authorizer Email L***@p**.com
Narrative At 1351 hours on february 27, 2015, pg&e was notified of a third-party dig-in near the intersection of elk grove-florin road and gerber road in sacramento. The third-party (western engineering) was using a backhoe to dig new underground services (sewer manholes) when they struck an 8-inch plastic distribution main, causing an unintentional release of natural gas. Western engineering provided a valid USA ticket (#413394). Pg&e facilities were properly located and marked, but the excavator failed to hand dig, expose, and protect the facilities before using mechanical equipment. Pg&e was onsite at 1405 hours. Gas was shut in by 1737 hours by excavating and squeezing the distribution main. Fire department, police, and sacramento media (channel 10 and 3) were observed on scene. Traffic was blocked on gerber road (east of elk grove-florin road) and rerouted from the area. The incident was reported to the cpuc and DOT due to damages likely exceeding $50,000. There were no injuries or fatalities reported. Additionally, there was no ignition and the estimated volume of gas released was less than three million cubic feet. Approximately 768 residential customers lost gas service during the incident. Pg&e restored gas service to all the available customers (I.E. Approximately 431 customers) by 0200 hours on february 28, 2015. By march 1, 2015, pg&e restored gas service for approximately 323 additional customers. As of march 26, 2015, service was restored for an additional eight customers; the remaining six homes are vacant.

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