HL incident on 2014-11-19 — TX

Operator
Sunoco Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2014-11-19 15:00
Report number
Location
TX
Narrative
Crude oil leaked from an underground flange connection that was not supported properly after installation in the ditch. The lack of proper support may have been a key contributing factor in the loosening of the flange bolts which ultimately led to the release. During line refill crude oil surfaced at this location and migrated into a drainage ditch that ultimately discharges into hawkins branch creek. Approximately one (1) gallon of crude oil impacted hawkins branch creek. After discovery of the release proper nrc and rrc notifications were made. All free oil was promptly cleaned up from the soil and water surfaces. The flanged connection was excavated, proper supporting fill material was installed in the ditch and the flange was re-torqued. The line was refilled, pressurized and checked for leakage. No further leakage was present and the line was returned to service.
Detailed record list
Report Received Date
2014-12-16 00:00:00
Iyear
2014
Report Number
20140426
Supplemental Number
20173
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-11-19 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-11-19 15:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Segment Already Down For Scheduled Maintenance.
On Site Datetime
2014-11-19 15:00:00
Nrc Rpt Datetime
2014-11-19 15:48:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Longview Gathering
Segment Name
612060-Longview Gathering-4-8" A
Onshore State Abbreviation
Tx
Onshore Postal Code
75693
Onshore City Name
White Oak
Onshore County Name
Gregg
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Interface Btn Poly & Carbon Steel Flange
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.1
Rel Water Name
Hawkins Branch Creek
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
2000
Est Cost Emergency
0
Est Cost Environmental
47458
Est Cost Other
0
Prpty
49508
Accident Psig
50
Mop Psig
125
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
6000
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
Yes
Qualified Individuals
No, But They Were Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2015-02-25 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
Crude oil leaked from an underground flange connection that was not supported properly after installation in the ditch. The lack of proper support may have been a key contributing factor in the loosening of the flange bolts which ultimately led to the release. During line refill crude oil surfaced at this location and migrated into a drainage ditch that ultimately discharges into hawkins branch creek. Approximately one (1) gallon of crude oil impacted hawkins branch creek. After discovery of the release proper nrc and rrc notifications were made. All free oil was promptly cleaned up from the soil and water surfaces. The flanged connection was excavated, proper supporting fill material was installed in the ditch and the flange was re-torqued. The line was refilled, pressurized and checked for leakage. No further leakage was present and the line was returned to service.
Report Received Date 2014-12-16 00:00:00
Iyear 2014
Report Number 20140426
Supplemental Number 20173
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-11-19 15:00:00
Location Latitude 32.53403 Google Maps OpenStreetMap
Location Longitude -94.84332 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-11-19 15:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Segment Already Down For Scheduled Maintenance.
On Site Datetime 2014-11-19 15:00:00
Nrc Rpt Datetime 2014-11-19 15:48:00
Nrc Rpt Num 1101483 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Longview Gathering
Segment Name 612060-Longview Gathering-4-8" A
Onshore State Abbreviation Tx
Onshore Postal Code 75693
Onshore City Name White Oak
Onshore County Name Gregg
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Interface Btn Poly & Carbon Steel Flange
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0.1
Rel Water Name Hawkins Branch Creek
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 2000
Est Cost Emergency 0
Est Cost Environmental 47458
Est Cost Other 0
Prpty 49508
Accident Psig 50
Mop Psig 125
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 6000
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind Yes
Qualified Individuals No, But They Were Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2015-02-25 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative Crude oil leaked from an underground flange connection that was not supported properly after installation in the ditch. The lack of proper support may have been a key contributing factor in the loosening of the flange bolts which ultimately led to the release. During line refill crude oil surfaced at this location and migrated into a drainage ditch that ultimately discharges into hawkins branch creek. Approximately one (1) gallon of crude oil impacted hawkins branch creek. After discovery of the release proper nrc and rrc notifications were made. All free oil was promptly cleaned up from the soil and water surfaces. The flanged connection was excavated, proper supporting fill material was installed in the ditch and the flange was re-torqued. The line was refilled, pressurized and checked for leakage. No further leakage was present and the line was returned to service.

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