HL incident on 2014-11-16 — TX

Operator
Central Florida Pipeline Corp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2014-11-16 08:25
Report number
Location
TX
Narrative
An employee performing a facility walk around noticed a small flame coming from a pressure sensing tubing line. The flame was extinguished by the employee. An investigation of the incident revealed the tubing had not been properly secured to the support after a previous tubing repair. The tubing had been secured to the conduit support bracket with electrical tape, allowing ac induced current on the pipeline to travel to ground via a pipe support around the pipeline insulating gasket. This resulted in electrical arching from the ac induced current on the pipeline and the tubing. The electrical arching resulted in a pinhole in the tubing and served as the ignition source for the flame.
Detailed record list
Report Received Date
2014-12-15 00:00:00
Iyear
2014
Report Number
20140423
Supplemental Number
20149
Report Type
Supplemental Final
Operator Id
Name
Central Florida Pipeline Corp
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-11-16 08:25:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-11-16 08:25:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-11-16 08:26:00
Restart Datetime
2014-11-17 18:29:00
On Site Datetime
2014-11-16 08:25:00
Nrc Rpt Datetime
2014-11-16 08:58:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Orlando Terminal
Segment Name
Orlando Terminal
Onshore State Abbreviation
Fl
Onshore Postal Code
32824
Onshore City Name
Orlando
Onshore County Name
Orange
Designated Location
Milepost/valve Station
Designated Name
Near Bv 24
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Tubing
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
1000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1000
Accident Psig
30
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident involved a pinhole in tubing and not related to pipeline operations.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
Q****** H* F******
Preparer Title
Manager Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-751-4240
Preparer Fax
770-751-4183
Prepared Date
2015-02-19 00:00:00
Authorizer Name
Q****** H* F******
Authorizer Telephone
770-751-4240
Authorizer Title
Manager Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
An employee performing a facility walk around noticed a small flame coming from a pressure sensing tubing line. The flame was extinguished by the employee. An investigation of the incident revealed the tubing had not been properly secured to the support after a previous tubing repair. The tubing had been secured to the conduit support bracket with electrical tape, allowing ac induced current on the pipeline to travel to ground via a pipe support around the pipeline insulating gasket. This resulted in electrical arching from the ac induced current on the pipeline and the tubing. The electrical arching resulted in a pinhole in the tubing and served as the ignition source for the flame.
Report Received Date 2014-12-15 00:00:00
Iyear 2014
Report Number 20140423
Supplemental Number 20149
Report Type Supplemental Final
Operator Id 2190 PHMSA Enforcement
Name Central Florida Pipeline Corp
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-11-16 08:25:00
Location Latitude 28.422698 Google Maps OpenStreetMap
Location Longitude -81.370474 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-11-16 08:25:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-11-16 08:26:00
Restart Datetime 2014-11-17 18:29:00
On Site Datetime 2014-11-16 08:25:00
Nrc Rpt Datetime 2014-11-16 08:58:00
Nrc Rpt Num 1101167 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Orlando Terminal
Segment Name Orlando Terminal
Onshore State Abbreviation Fl
Onshore Postal Code 32824
Onshore City Name Orlando
Onshore County Name Orange
Designated Location Milepost/valve Station
Designated Name Near Bv 24
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Tubing
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 1000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1000
Accident Psig 30
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident involved a pinhole in tubing and not related to pipeline operations.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name Q****** H* F******
Preparer Title Manager Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-751-4240
Preparer Fax 770-751-4183
Prepared Date 2015-02-19 00:00:00
Authorizer Name Q****** H* F******
Authorizer Telephone 770-751-4240
Authorizer Title Manager Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative An employee performing a facility walk around noticed a small flame coming from a pressure sensing tubing line. The flame was extinguished by the employee. An investigation of the incident revealed the tubing had not been properly secured to the support after a previous tubing repair. The tubing had been secured to the conduit support bracket with electrical tape, allowing ac induced current on the pipeline to travel to ground via a pipe support around the pipeline insulating gasket. This resulted in electrical arching from the ac induced current on the pipeline and the tubing. The electrical arching resulted in a pinhole in the tubing and served as the ignition source for the flame.

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