HL incident on 2014-11-07 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2014-11-07 07:13
Report number
Location
TX
Narrative
On november 7 at approximately 7:12 a.M., edmonton control center received a leak detection alarm from the lockport-mustang densitometer building and contacted the on-site gauger. He immediately investigated and discovered that a release took place around the densitometer cabinet release. He then contacted the station technician, who was also on-site. Line 6a was immediately shutdown. It was discovered that there was an internal coupling failure within the densitometer magnetic drive pump resulting in sudden, forceful wear and failure of the canister. A new motor and pump was installed and the line was restarted later that morning. Approximately 30 cubic yards of contaminated soil was removed from the site.
Detailed record list
Report Received Date
2014-12-05 00:00:00
Iyear
2014
Report Number
20140412
Supplemental Number
19940
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2014-11-07 07:12:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-11-07 07:13:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-11-07 07:13:00
Restart Datetime
2014-11-07 09:08:00
On Site Datetime
2014-11-07 07:13:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lm
Segment Name
Mustang Densitometer
Onshore State Abbreviation
Il
Onshore Postal Code
60441
Onshore City Name
Lockport
Onshore County Name
Will
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Other
Leak Type Other
Mechanical Wear
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
31
Est Cost Prop Damage
6000
Est Cost Emergency
11220
Est Cost Environmental
15140
Est Cost Other
0
Prpty
32391
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2014-12-05 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
On november 7 at approximately 7:12 a.M., edmonton control center received a leak detection alarm from the lockport-mustang densitometer building and contacted the on-site gauger. He immediately investigated and discovered that a release took place around the densitometer cabinet release. He then contacted the station technician, who was also on-site. Line 6a was immediately shutdown. It was discovered that there was an internal coupling failure within the densitometer magnetic drive pump resulting in sudden, forceful wear and failure of the canister. A new motor and pump was installed and the line was restarted later that morning. Approximately 30 cubic yards of contaminated soil was removed from the site.
Report Received Date 2014-12-05 00:00:00
Iyear 2014
Report Number 20140412
Supplemental Number 19940
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2014-11-07 07:12:00
Location Latitude 41.63611 Google Maps OpenStreetMap
Location Longitude -88.04639 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-11-07 07:13:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-11-07 07:13:00
Restart Datetime 2014-11-07 09:08:00
On Site Datetime 2014-11-07 07:13:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lm
Segment Name Mustang Densitometer
Onshore State Abbreviation Il
Onshore Postal Code 60441
Onshore City Name Lockport
Onshore County Name Will
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Pump
Release Type Leak
Leak Type Other
Leak Type Other Mechanical Wear
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 31
Est Cost Prop Damage 6000
Est Cost Emergency 11220
Est Cost Environmental 15140
Est Cost Other 0
Prpty 32391
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2014-12-05 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative On november 7 at approximately 7:12 a.M., edmonton control center received a leak detection alarm from the lockport-mustang densitometer building and contacted the on-site gauger. He immediately investigated and discovered that a release took place around the densitometer cabinet release. He then contacted the station technician, who was also on-site. Line 6a was immediately shutdown. It was discovered that there was an internal coupling failure within the densitometer magnetic drive pump resulting in sudden, forceful wear and failure of the canister. A new motor and pump was installed and the line was restarted later that morning. Approximately 30 cubic yards of contaminated soil was removed from the site.

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