HL incident on 2014-11-01 — TX

Operator
Sunoco Pipeline L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$19,000
Incident datetime
2014-11-01 15:45
Report number
Location
TX
Narrative
On 10/31/2014 the dover to hennessey pipeline was shut down by the control center due to an over/short line imbalance. Air patrol was dispatched, flew the line and reported no visible signs of a release. The line remained shut down overnight. On 11/1/2014 a pressure integrity check of the pipeline was initiated and aborted when the line did not hold pressure. Foot patrol along the line on 11/1/2014 identified and confirmed the point of release. The release site was excavated, the line was purged and the failed section of pipe was cut out and replaced. The line was subsequently successfully hydrostatically pressure tested. The line was placed back into service on 11/7/2014. On january 23, 2015 it was determined that remediation costs would cause total costs to exceed $50,000. Therefore an nrc notification was made per the requirement defined under 195.52(a)(3). Metallurgical analysis revealed that the failure was the result of a pre-existing weld flaw produced in the pipe mill during manufacture.
Detailed record list
Report Received Date
2014-12-01 00:00:00
Iyear
2014
Report Number
20140408
Supplemental Number
20330
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-11-01 15:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2014-11-01 15:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-11-01 15:45:00
Restart Datetime
2014-11-07 15:00:00
On Site Datetime
2014-11-01 15:45:00
Nrc Rpt Datetime
2015-01-23 10:40:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Dover To Hennessey 4"
Segment Name
541003-4" Dover To Hennessey
Onshore State Abbreviation
Ok
Onshore Postal Code
73750
Onshore City Name
Kingfisher
Onshore County Name
Kingfisher
Designated Location
Milepost/valve Station
Designated Name
1
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
4.5
Pipe Wall Thickness
0.156
Pipe Smys
30000
Pipe Specification
Grade A
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
Unknown
Manufactured Year
1950
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
21500
Est Cost Gas Released
1000
Est Cost Prop Damage
19000
Est Cost Emergency
2500
Est Cost Environmental
380000
Est Cost Other
0
Prpty
424000
Accident Psig
624
Mop Psig
714
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
28381
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Pre-Existing Weld Flaw In The Pipe Mill During Manufacture.
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2011
Other Recent Year
2011
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2001
Hydrtst Most Rcnt Pressure
893
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2015-04-13 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 10/31/2014 the dover to hennessey pipeline was shut down by the control center due to an over/short line imbalance. Air patrol was dispatched, flew the line and reported no visible signs of a release. The line remained shut down overnight. On 11/1/2014 a pressure integrity check of the pipeline was initiated and aborted when the line did not hold pressure. Foot patrol along the line on 11/1/2014 identified and confirmed the point of release. The release site was excavated, the line was purged and the failed section of pipe was cut out and replaced. The line was subsequently successfully hydrostatically pressure tested. The line was placed back into service on 11/7/2014. On january 23, 2015 it was determined that remediation costs would cause total costs to exceed $50,000. Therefore an nrc notification was made per the requirement defined under 195.52(a)(3). Metallurgical analysis revealed that the failure was the result of a pre-existing weld flaw produced in the pipe mill during manufacture.
Report Received Date 2014-12-01 00:00:00
Iyear 2014
Report Number 20140408
Supplemental Number 20330
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-11-01 15:45:00
Location Latitude 36.04031 Google Maps OpenStreetMap
Location Longitude -97.91048 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2014-11-01 15:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-11-01 15:45:00
Restart Datetime 2014-11-07 15:00:00
On Site Datetime 2014-11-01 15:45:00
Nrc Rpt Datetime 2015-01-23 10:40:00
Nrc Rpt Num 1106401 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Dover To Hennessey 4"
Segment Name 541003-4" Dover To Hennessey
Onshore State Abbreviation Ok
Onshore Postal Code 73750
Onshore City Name Kingfisher
Onshore County Name Kingfisher
Designated Location Milepost/valve Station
Designated Name 1
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 4.5
Pipe Wall Thickness 0.156
Pipe Smys 30000
Pipe Specification Grade A
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year Unknown
Manufactured Year 1950
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 21500
Est Cost Gas Released 1000
Est Cost Prop Damage 19000
Est Cost Emergency 2500
Est Cost Environmental 380000
Est Cost Other 0
Prpty 424000
Accident Psig 624
Mop Psig 714
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 28381
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Pre-Existing Weld Flaw In The Pipe Mill During Manufacture.
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2011
Other Recent Year 2011
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2001
Hydrtst Most Rcnt Pressure 893
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2015-04-13 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 10/31/2014 the dover to hennessey pipeline was shut down by the control center due to an over/short line imbalance. Air patrol was dispatched, flew the line and reported no visible signs of a release. The line remained shut down overnight. On 11/1/2014 a pressure integrity check of the pipeline was initiated and aborted when the line did not hold pressure. Foot patrol along the line on 11/1/2014 identified and confirmed the point of release. The release site was excavated, the line was purged and the failed section of pipe was cut out and replaced. The line was subsequently successfully hydrostatically pressure tested. The line was placed back into service on 11/7/2014. On january 23, 2015 it was determined that remediation costs would cause total costs to exceed $50,000. Therefore an nrc notification was made per the requirement defined under 195.52(a)(3). Metallurgical analysis revealed that the failure was the result of a pre-existing weld flaw produced in the pipe mill during manufacture.

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