HL incident on 2014-11-01 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2014-11-01 17:00
Report number
Location
TX
Narrative
During evening rounds on november 1, 2014 at approximately 5:00 pm, a leak was discovered within the griffith terminal manifold originating from the stem seal of manifold valve 750. The valve was locked out and the terminal staff promptly performed cleanup and monitored the valve. The repair will require an extensive outage that is not yet scheduled. Approximately 5 gallons were released prior to discovery and were completely contained within the immediate area of the valve. Approximately 0.27 cubic yards of contaminated gravel and road mix was removed from the site.
Detailed record list
Report Received Date
2014-12-01 00:00:00
Iyear
2014
Report Number
20140406
Supplemental Number
19926
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2014-11-01 17:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-11-01 17:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Locked Out. Release Had No Impact To Operations.
On Site Datetime
2014-11-01 17:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Gt
Segment Name
Griffith Manifold
Onshore State Abbreviation
In
Onshore Postal Code
46319
Onshore City Name
Griffith
Onshore County Name
Lake
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
2
Est Cost Prop Damage
3000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
3002
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2014-12-01 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
During evening rounds on november 1, 2014 at approximately 5:00 pm, a leak was discovered within the griffith terminal manifold originating from the stem seal of manifold valve 750. The valve was locked out and the terminal staff promptly performed cleanup and monitored the valve. The repair will require an extensive outage that is not yet scheduled. Approximately 5 gallons were released prior to discovery and were completely contained within the immediate area of the valve. Approximately 0.27 cubic yards of contaminated gravel and road mix was removed from the site.
Report Received Date 2014-12-01 00:00:00
Iyear 2014
Report Number 20140406
Supplemental Number 19926
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2014-11-01 17:00:00
Location Latitude 41.51556 Google Maps OpenStreetMap
Location Longitude -87.44861 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-11-01 17:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Locked Out. Release Had No Impact To Operations.
On Site Datetime 2014-11-01 17:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Gt
Segment Name Griffith Manifold
Onshore State Abbreviation In
Onshore Postal Code 46319
Onshore City Name Griffith
Onshore County Name Lake
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 2
Est Cost Prop Damage 3000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 3002
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2014-12-01 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative During evening rounds on november 1, 2014 at approximately 5:00 pm, a leak was discovered within the griffith terminal manifold originating from the stem seal of manifold valve 750. The valve was locked out and the terminal staff promptly performed cleanup and monitored the valve. The repair will require an extensive outage that is not yet scheduled. Approximately 5 gallons were released prior to discovery and were completely contained within the immediate area of the valve. Approximately 0.27 cubic yards of contaminated gravel and road mix was removed from the site.

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