HL incident on 2014-10-28 — TX

Operator
Rose Rock Midstream L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2014-10-28 03:21
Report number
Location
TX
Narrative
The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls.
Detailed record list
Report Received Date
2014-11-30 00:00:00
Iyear
2014
Report Number
20140405
Supplemental Number
19939
Report Type
Supplemental Final
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-10-28 03:21:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-10-28 03:21:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-10-28 03:21:00
Restart Datetime
2014-10-28 05:00:00
On Site Datetime
2014-10-28 03:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing West 20"
Segment Name
West 20"
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
2000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2100
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
E*** N********
Preparer Title
District Manager
Preparer Email
E*********@s***********.com
Preparer Telephone
918-225-7758
Preparer Fax
918-225-2579
Prepared Date
2014-12-05 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
918-524-8109
Authorizer Title
Dot Compliance Specialist Sr
Authorizer Email
T********@s***********.com
Narrative
The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls.
Report Received Date 2014-11-30 00:00:00
Iyear 2014
Report Number 20140405
Supplemental Number 19939
Report Type Supplemental Final
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-10-28 03:21:00
Location Latitude 35.982628 Google Maps OpenStreetMap
Location Longitude -96.764171 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-10-28 03:21:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-10-28 03:21:00
Restart Datetime 2014-10-28 05:00:00
On Site Datetime 2014-10-28 03:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing West 20"
Segment Name West 20"
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name 1
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Flange Assembly
Release Type Leak
Leak Type Other
Leak Type Other Gasket
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 2000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2100
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name E*** N********
Preparer Title District Manager
Preparer Email E*********@s***********.com
Preparer Telephone 918-225-7758
Preparer Fax 918-225-2579
Prepared Date 2014-12-05 00:00:00
Authorizer Name T*** A*******
Authorizer Telephone 918-524-8109
Authorizer Title Dot Compliance Specialist Sr
Authorizer Email T********@s***********.com
Narrative The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls.

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