Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-10-28 — TX
Operator
Rose Rock Midstream L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,000
Incident datetime
2014-10-28 03:21
Report number
Location
TX
Narrative
The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls.
Detailed record list
Report Received Date
2014-11-30 00:00:00
Iyear
2014
Report Number
20140405
Supplemental Number
19939
Report Type
Supplemental Final
Operator Id
31476
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-10-28 03:21:00
Location Latitude
35.982628
Location Longitude
-96.764171
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-10-28 03:21:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-10-28 03:21:00
Restart Datetime
2014-10-28 05:00:00
On Site Datetime
2014-10-28 03:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing West 20"
Segment Name
West 20"
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
2000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2100
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
E*** N********
Preparer Title
District Manager
Preparer Email
E*********@s***********.com
Preparer Telephone
918-225-7758
Preparer Fax
918-225-2579
Prepared Date
2014-12-05 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
918-524-8109
Authorizer Title
Dot Compliance Specialist Sr
Authorizer Email
T********@s***********.com
Narrative
The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls.
| Report Received Date | 2014-11-30 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140405 |
| Supplemental Number | 19939 |
| Report Type | Supplemental Final |
| Operator Id | 31476 PHMSA Enforcement |
| Name | Rose Rock Midstream L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2014-10-28 03:21:00 |
| Location Latitude | 35.982628 Google Maps OpenStreetMap |
| Location Longitude | -96.764171 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-10-28 03:21:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2014-10-28 03:21:00 |
| Restart Datetime | 2014-10-28 05:00:00 |
| On Site Datetime | 2014-10-28 03:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Cushing West 20" |
| Segment Name | West 20" |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 74023 |
| Onshore City Name | Cushing |
| Onshore County Name | Payne |
| Designated Location | Milepost/valve Station |
| Designated Name | 1 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Flange Assembly |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Gasket |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 100 |
| Est Cost Prop Damage | 2000 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2100 |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Operation Type | Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure |
| Preparer Name | E*** N******** |
| Preparer Title | District Manager |
| Preparer Email | E*********@s***********.com |
| Preparer Telephone | 918-225-7758 |
| Preparer Fax | 918-225-2579 |
| Prepared Date | 2014-12-05 00:00:00 |
| Authorizer Name | T*** A******* |
| Authorizer Telephone | 918-524-8109 |
| Authorizer Title | Dot Compliance Specialist Sr |
| Authorizer Email | T********@s***********.com |
| Narrative | The cushing operator / okc control center was in the process of starting up a delivery to enterprise at the west cushing terminal. Enterprise failed to provide an open path and subsequently caused a high pressure shutdown on the mainline unit. This pressure situation caused a flange to leak at the scraper trap causing a spill of less than 2 bbls. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA