HL incident on 2014-10-18 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2014-10-18 12:56
Report number
Location
TX
Narrative
On 10/18/2014 a member of the public notified the sour lake office of a sump overflow at the black cat road scraper trap. The control center was immediately notified and the line segment was shut down and operations personnel were dispatched to the location. Investigation revealed that a 2" ball valve was leaking around the rubber seat allowing crude oil to enter the sump. The ball valve was deemed unnecessary to the current operation and was removed and a plug installed in the fitting.
Detailed record list
Report Received Date
2014-11-17 00:00:00
Iyear
2014
Report Number
20140398
Supplemental Number
19905
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-10-18 12:56:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2014-10-18 12:56:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-10-18 12:56:00
Restart Datetime
2014-10-18 18:31:00
On Site Datetime
2014-10-18 13:10:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Blackcat Scraper Trap
Segment Name
21016-Saratoga To Sour Lake 6/8"
Onshore State Abbreviation
Tx
Onshore Postal Code
77659
Onshore City Name
Sour Lake
Onshore County Name
Hardin
Designated Location
Survey Station No.
Designated Name
460+46
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
238
Est Cost Prop Damage
50
Est Cost Emergency
5000
Est Cost Environmental
1250
Est Cost Other
0
Prpty
6538
Accident Psig
100
Mop Psig
150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
17952
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2014-11-17 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 10/18/2014 a member of the public notified the sour lake office of a sump overflow at the black cat road scraper trap. The control center was immediately notified and the line segment was shut down and operations personnel were dispatched to the location. Investigation revealed that a 2" ball valve was leaking around the rubber seat allowing crude oil to enter the sump. The ball valve was deemed unnecessary to the current operation and was removed and a plug installed in the fitting.
Report Received Date 2014-11-17 00:00:00
Iyear 2014
Report Number 20140398
Supplemental Number 19905
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-10-18 12:56:00
Location Latitude 30.18148 Google Maps OpenStreetMap
Location Longitude -94.42918 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2014-10-18 12:56:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-10-18 12:56:00
Restart Datetime 2014-10-18 18:31:00
On Site Datetime 2014-10-18 13:10:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Blackcat Scraper Trap
Segment Name 21016-Saratoga To Sour Lake 6/8"
Onshore State Abbreviation Tx
Onshore Postal Code 77659
Onshore City Name Sour Lake
Onshore County Name Hardin
Designated Location Survey Station No.
Designated Name 460+46
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 238
Est Cost Prop Damage 50
Est Cost Emergency 5000
Est Cost Environmental 1250
Est Cost Other 0
Prpty 6538
Accident Psig 100
Mop Psig 150
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 17952
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Wear
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2014-11-17 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 10/18/2014 a member of the public notified the sour lake office of a sump overflow at the black cat road scraper trap. The control center was immediately notified and the line segment was shut down and operations personnel were dispatched to the location. Investigation revealed that a 2" ball valve was leaking around the rubber seat allowing crude oil to enter the sump. The ball valve was deemed unnecessary to the current operation and was removed and a plug installed in the fitting.

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