Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-10-25 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2014-10-25 09:03
Report number
Location
TX
Narrative
At 8:44 p66pl controller began start up of powder river ngl line. At 9:03 b.C.C. Received a hazardous atmosphere high alarm immediately followed by hazardous atmosphere high high and station esd alarms. P66pl controller blocked in the unit adjusted the line to run without the station and called field personnel to investigate. 11:35 field personnel arrived at kerrick station and found bad seals on unit 2. Field personnel fully isolated and depressured the unit 2 pump. In order to prevent reoccurrance, p66pl modify the seal flush supply to increase supply pressure by moving to the fourth stage discharge. In addition, the flush location is being changed to better balance the seal. These changes along with a replacement seal have been implemented and the unit 2 pump is now back in service.
Detailed record list
Report Received Date
2014-11-17 00:00:00
Iyear
2014
Report Number
20140397
Supplemental Number
19904
Report Type
Original Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2014-10-25 09:03:00
Location Latitude
36.472798
Location Longitude
-102.268817
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.17
Intentional Release Bbls
3.3
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-10-25 09:03:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Seal Leak; Station Was Bypassed And Pipeline Continued To Operate
On Site Datetime
2014-10-25 11:35:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Powder River/kerrick Station
Segment Name
Pr-01
Onshore State Abbreviation
Tx
Onshore Postal Code
79051
Onshore County Name
Dallam
Designated Location
Milepost/valve Station
Designated Name
Kerrick
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
5060
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
C**** F*****
Preparer Title
Dot Coordinator
Preparer Email
C*************@p**.com
Preparer Telephone
303-862-1189
Preparer Fax
918-977-8545
Prepared Date
2014-11-17 00:00:00
Authorizer Name
T*** T*****
Authorizer Telephone
8327651636
Authorizer Title
Mgr. Regulatory Compliance
Authorizer Email
T************@p**.com
Narrative
At 8:44 p66pl controller began start up of powder river ngl line. At 9:03 b.C.C. Received a hazardous atmosphere high alarm immediately followed by hazardous atmosphere high high and station esd alarms. P66pl controller blocked in the unit adjusted the line to run without the station and called field personnel to investigate. 11:35 field personnel arrived at kerrick station and found bad seals on unit 2. Field personnel fully isolated and depressured the unit 2 pump. In order to prevent reoccurrance, p66pl modify the seal flush supply to increase supply pressure by moving to the fourth stage discharge. In addition, the flush location is being changed to better balance the seal. These changes along with a replacement seal have been implemented and the unit 2 pump is now back in service.
| Report Received Date | 2014-11-17 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140397 |
| Supplemental Number | 19904 |
| Report Type | Original Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2014-10-25 09:03:00 |
| Location Latitude | 36.472798 Google Maps OpenStreetMap |
| Location Longitude | -102.268817 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 0.17 |
| Intentional Release Bbls | 3.3 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-10-25 09:03:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Pump Seal Leak; Station Was Bypassed And Pipeline Continued To Operate |
| On Site Datetime | 2014-10-25 11:35:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Powder River/kerrick Station |
| Segment Name | Pr-01 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79051 |
| Onshore County Name | Dallam |
| Designated Location | Milepost/valve Station |
| Designated Name | Kerrick |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 60 |
| Est Cost Prop Damage | 5000 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 5060 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | C**** F***** |
| Preparer Title | Dot Coordinator |
| Preparer Email | C*************@p**.com |
| Preparer Telephone | 303-862-1189 |
| Preparer Fax | 918-977-8545 |
| Prepared Date | 2014-11-17 00:00:00 |
| Authorizer Name | T*** T***** |
| Authorizer Telephone | 8327651636 |
| Authorizer Title | Mgr. Regulatory Compliance |
| Authorizer Email | T************@p**.com |
| Narrative | At 8:44 p66pl controller began start up of powder river ngl line. At 9:03 b.C.C. Received a hazardous atmosphere high alarm immediately followed by hazardous atmosphere high high and station esd alarms. P66pl controller blocked in the unit adjusted the line to run without the station and called field personnel to investigate. 11:35 field personnel arrived at kerrick station and found bad seals on unit 2. Field personnel fully isolated and depressured the unit 2 pump. In order to prevent reoccurrance, p66pl modify the seal flush supply to increase supply pressure by moving to the fourth stage discharge. In addition, the flush location is being changed to better balance the seal. These changes along with a replacement seal have been implemented and the unit 2 pump is now back in service. |
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