HL incident on 2014-10-18 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$37,000
Incident datetime
2014-10-18 04:18
Report number
Location
TX
Narrative
The operator smelled gas in pit 3 area and a leak was found upon investigation. The top of pipe was leaking gas and the inbound pipeline was immediately shut down. Line was isolated from the tank and pit until permanent repairs can be made.
Detailed record list
Report Received Date
2014-11-14 00:00:00
Iyear
2014
Report Number
20140396
Supplemental Number
20553
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-10-18 04:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2
Recovered Bbls
1.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-10-18 04:18:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-10-18 04:20:00
Restart Datetime
2014-10-18 11:24:00
On Site Datetime
2014-10-18 04:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pasadena Terminal
Segment Name
150-13 Back Door Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77506-0351
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
Unknown
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
37000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
37000
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Local operation independent of the controller, discovered during the walk around.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Atmosphere Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2014
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D******* S*******
Preparer Title
Director
Preparer Email
D****************@k***********.com
Preparer Telephone
7137250147
Prepared Date
2015-06-25 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
7137250147
Authorizer Title
Director
Authorizer Email
D****************@k***********.com
Narrative
The operator smelled gas in pit 3 area and a leak was found upon investigation. The top of pipe was leaking gas and the inbound pipeline was immediately shut down. Line was isolated from the tank and pit until permanent repairs can be made.
Report Received Date 2014-11-14 00:00:00
Iyear 2014
Report Number 20140396
Supplemental Number 20553
Report Type Supplemental Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-10-18 04:20:00
Location Latitude 29.73064 Google Maps OpenStreetMap
Location Longitude -95.20349 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2
Recovered Bbls 1.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-10-18 04:18:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-10-18 04:20:00
Restart Datetime 2014-10-18 11:24:00
On Site Datetime 2014-10-18 04:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Pasadena Terminal
Segment Name 150-13 Back Door Line
Onshore State Abbreviation Tx
Onshore Postal Code 77506-0351
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness Unknown
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 37000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 37000
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Local operation independent of the controller, discovered during the walk around.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Atmosphere Corrosion Ind Yes
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2014
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D******* S*******
Preparer Title Director
Preparer Email D****************@k***********.com
Preparer Telephone 7137250147
Prepared Date 2015-06-25 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 7137250147
Authorizer Title Director
Authorizer Email D****************@k***********.com
Narrative The operator smelled gas in pit 3 area and a leak was found upon investigation. The top of pipe was leaking gas and the inbound pipeline was immediately shut down. Line was isolated from the tank and pit until permanent repairs can be made.

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