HL incident on 2014-09-24 — TX

Operator
Exxonmobil Pipeline Co
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2014-09-24 10:00
Report number
Location
TX
Narrative
Investigation of the incident remains ongoing. The affected right-of-way contains a third-party pipeline, which also transports refined products. Sampling data of the impacted soils appears inconsistent with a release of product from empco's pipeline. It is unclear at this point whether the subject pinhole anomaly was through-wall prior to sandblasting and cleaning for examination. At this point, it appears the release impacted mainly soil, but intermittent light sheens were observed on an apparent man-made impoundment on santa clara creek, guadalupe county, texas. The pipeline was shut down at 06:15 9/24/14 in the course of normal business. The release was discovered at approximately 10:00 9/24/14. The pipeline was repaired utilizing a full encirclement welded sleeve.
Detailed record list
Report Received Date
2014-10-24 00:00:00
Iyear
2014
Report Number
20140376
Supplemental Number
19830
Report Type
Original
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
800 Bell Street, Rm 623f
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-09-24 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
15
Recovered Bbls
6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2014-09-24 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Shut Down At 06:15 09/24/14 In The Course Of Normal Business.
On Site Datetime
2014-09-24 10:00:00
Nrc Rpt Datetime
2014-09-24 13:48:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Baytown To San Antonio Refined Products Pipeline
Segment Name
Mcqueeny To San Antonio
Onshore State Abbreviation
Tx
Onshore Postal Code
78124
Onshore City Name
Marion
Onshore County Name
Guadalupe
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
X52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Textube
Pipe Coating Type
Coal Tar
Installation Year
1962
Manufactured Year
1962
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0
Rel Water Name
An Apparent Manmade Impoundment On Santa Clara Creek, Slight Sheen Only
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2000
Est Cost Prop Damage
10000
Est Cost Emergency
100000
Est Cost Environmental
650000
Est Cost Other
0
Prpty
762000
Accident Psig
35
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
108900
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a pinhole type leak that is below the leak detection threshold for empco's current scada system.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Localized Pit
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1991
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2014
Close Interval Survey Year
2014
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2014
Geometry Recent Year
2014
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1994
Hydrtst Most Rcnt Pressure
1956
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** M*********
Preparer Title
Pipeline Safety Advisor
Preparer Email
T**************@e*********.com
Preparer Telephone
8326247880
Preparer Fax
7136568232
Prepared Date
2014-10-24 00:00:00
Authorizer Name
J** B* R***
Authorizer Telephone
8326254920
Authorizer Title
Sshe Manager
Authorizer Email
J*********@e*********.com
Narrative
Investigation of the incident remains ongoing. The affected right-of-way contains a third-party pipeline, which also transports refined products. Sampling data of the impacted soils appears inconsistent with a release of product from empco's pipeline. It is unclear at this point whether the subject pinhole anomaly was through-wall prior to sandblasting and cleaning for examination. At this point, it appears the release impacted mainly soil, but intermittent light sheens were observed on an apparent man-made impoundment on santa clara creek, guadalupe county, texas. The pipeline was shut down at 06:15 9/24/14 in the course of normal business. The release was discovered at approximately 10:00 9/24/14. The pipeline was repaired utilizing a full encirclement welded sleeve.
Report Received Date 2014-10-24 00:00:00
Iyear 2014
Report Number 20140376
Supplemental Number 19830
Report Type Original
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 800 Bell Street, Rm 623f
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-09-24 10:00:00
Location Latitude 29.56687 Google Maps OpenStreetMap
Location Longitude -98.12972 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 15
Recovered Bbls 6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2014-09-24 10:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Shut Down At 06:15 09/24/14 In The Course Of Normal Business.
On Site Datetime 2014-09-24 10:00:00
Nrc Rpt Datetime 2014-09-24 13:48:00
Nrc Rpt Num 1096347 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Baytown To San Antonio Refined Products Pipeline
Segment Name Mcqueeny To San Antonio
Onshore State Abbreviation Tx
Onshore Postal Code 78124
Onshore City Name Marion
Onshore County Name Guadalupe
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification X52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Textube
Pipe Coating Type Coal Tar
Installation Year 1962
Manufactured Year 1962
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 0
Rel Water Name An Apparent Manmade Impoundment On Santa Clara Creek, Slight Sheen Only
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2000
Est Cost Prop Damage 10000
Est Cost Emergency 100000
Est Cost Environmental 650000
Est Cost Other 0
Prpty 762000
Accident Psig 35
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 108900
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a pinhole type leak that is below the leak detection threshold for empco's current scada system.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Localized Pit
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1991
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2014
Close Interval Survey Year 2014
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2014
Geometry Recent Year 2014
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1994
Hydrtst Most Rcnt Pressure 1956
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** M*********
Preparer Title Pipeline Safety Advisor
Preparer Email T**************@e*********.com
Preparer Telephone 8326247880
Preparer Fax 7136568232
Prepared Date 2014-10-24 00:00:00
Authorizer Name J** B* R***
Authorizer Telephone 8326254920
Authorizer Title Sshe Manager
Authorizer Email J*********@e*********.com
Narrative Investigation of the incident remains ongoing. The affected right-of-way contains a third-party pipeline, which also transports refined products. Sampling data of the impacted soils appears inconsistent with a release of product from empco's pipeline. It is unclear at this point whether the subject pinhole anomaly was through-wall prior to sandblasting and cleaning for examination. At this point, it appears the release impacted mainly soil, but intermittent light sheens were observed on an apparent man-made impoundment on santa clara creek, guadalupe county, texas. The pipeline was shut down at 06:15 9/24/14 in the course of normal business. The release was discovered at approximately 10:00 9/24/14. The pipeline was repaired utilizing a full encirclement welded sleeve.

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