HL incident on 2014-09-25 — KS

Operator
Koch Pipeline Company, L.p.
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-09-25 09:15
Report number
Location
KS
Narrative
On september 25, 2014 at 9:15 a.M., koch pipeline company ("kpl") located a small release on the minnesota pipe line 2 ("mpl 2") loop 7 pipeline segment from zimmerman to hugo, and more specifically located near milepost 218 during a hydrostatic test. At the time of the hydrostatic test, the line was not connected to the main pipeline and was being monitored locally and not by the pipeline control center. The location of the release was determined to be within a jurisdictional wetland, although at the time of the release the wetland was dry and no surface waters were impacted. Due to this area being a jurisdictional wetland, it is considered a release to surface water, but since the wetland was dry at the time, the only known impact was to soil. A metallurgical investigation of the pipe concluded that the cause of the test failure (near mp218) was a manufacturing defect, a through wall lack of fusion in the longitudinal seam. The failure occurred during the spike test, at pressure higher than the original pipe mill test pressure, with no indication of fatigue growth. Approximately 2,000 gallons of hydrostatic test water with a small amount of residual crude oil were released. Through third party sampling, it was estimated that 88-165 gallons of crude oil were released along with the hydrostatic test water. Upon discovery, the pipeline was immediately clamped to stop leakage, cleanup was initiated, and necessary repairs were undertaken. All contaminated soil was removed off site to be treated and clean backfill soil was replaced in the excavation. The total amount of soil remediated was approximately 915 tons.
Detailed record list
Report Received Date
2014-10-24 00:00:00
Iyear
2014
Report Number
20140374
Supplemental Number
20755
Report Type
Supplemental Final
Operator Id
Name
Koch Pipeline Company, L.p.
Operator Street Address
4111 East 37th Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2014-09-25 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3.93
Recovered Bbls
3.93
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-09-25 09:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Section Was Disconnected From The Active Pipeline System.
On Site Datetime
2014-09-25 09:15:00
Nrc Rpt Datetime
2014-09-25 10:40:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Minnesota Pipeline 2
Segment Name
Zimmerman To Hugo
Onshore State Abbreviation
Mn
Onshore Postal Code
55014
Onshore City Name
Lino Lakes
Onshore County Name
Anoka
Designated Location
Milepost/valve Station
Designated Name
218
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
54
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
Api 5lx
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Interprovincial Pipe Corporation
Pipe Coating Type
Cold Applied Tape
Installation Year
1973
Manufactured Year
1973
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
3.93
Rel Water Name
Unnamed Jurisdictional Wetland Dry During Release And Cleanup
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
368
Est Cost Prop Damage
0
Est Cost Emergency
93204
Est Cost Environmental
0
Est Cost Other
922664
Est Cost Other Details
Cost To Investigate/locate Pinhole On Approx. 14 Miles Of Pipeline Segment.
Prpty
1016236
Accident Psig
1614
Mop Psig
1170
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Length Segment Isolated
47520
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Hydrostatic Pressure Test
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Ultrasonic Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Axial Recent Year
2006
Ultrasonic Recent Year
2008
Geometry Recent Year
2006
Emat Recent Year
2009
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2014
Hydrtst Most Rcnt Pressure
1614
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C**** K*******
Preparer Title
Program Specialist
Preparer Email
C*************@k***********.com
Preparer Telephone
316-828-4121
Preparer Fax
316-529-6377
Prepared Date
2015-09-21 00:00:00
Authorizer Name
K** G*****
Authorizer Telephone
651-438-1775
Authorizer Title
Dot Compliance Specialist
Authorizer Email
K*********@k***********.com
Narrative
On september 25, 2014 at 9:15 a.M., koch pipeline company ("kpl") located a small release on the minnesota pipe line 2 ("mpl 2") loop 7 pipeline segment from zimmerman to hugo, and more specifically located near milepost 218 during a hydrostatic test. At the time of the hydrostatic test, the line was not connected to the main pipeline and was being monitored locally and not by the pipeline control center. The location of the release was determined to be within a jurisdictional wetland, although at the time of the release the wetland was dry and no surface waters were impacted. Due to this area being a jurisdictional wetland, it is considered a release to surface water, but since the wetland was dry at the time, the only known impact was to soil. A metallurgical investigation of the pipe concluded that the cause of the test failure (near mp218) was a manufacturing defect, a through wall lack of fusion in the longitudinal seam. The failure occurred during the spike test, at pressure higher than the original pipe mill test pressure, with no indication of fatigue growth. Approximately 2,000 gallons of hydrostatic test water with a small amount of residual crude oil were released. Through third party sampling, it was estimated that 88-165 gallons of crude oil were released along with the hydrostatic test water. Upon discovery, the pipeline was immediately clamped to stop leakage, cleanup was initiated, and necessary repairs were undertaken. All contaminated soil was removed off site to be treated and clean backfill soil was replaced in the excavation. The total amount of soil remediated was approximately 915 tons.
Report Received Date 2014-10-24 00:00:00
Iyear 2014
Report Number 20140374
Supplemental Number 20755
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Koch Pipeline Company, L.p.
Operator Street Address 4111 East 37th Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2014-09-25 09:15:00
Location Latitude 45.206089 Google Maps OpenStreetMap
Location Longitude -93.099272 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3.93
Recovered Bbls 3.93
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-09-25 09:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Section Was Disconnected From The Active Pipeline System.
On Site Datetime 2014-09-25 09:15:00
Nrc Rpt Datetime 2014-09-25 10:40:00
Nrc Rpt Num 1096428 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Minnesota Pipeline 2
Segment Name Zimmerman To Hugo
Onshore State Abbreviation Mn
Onshore Postal Code 55014
Onshore City Name Lino Lakes
Onshore County Name Anoka
Designated Location Milepost/valve Station
Designated Name 218
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 54
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 16
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification Api 5lx
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Interprovincial Pipe Corporation
Pipe Coating Type Cold Applied Tape
Installation Year 1973
Manufactured Year 1973
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 3.93
Rel Water Name Unnamed Jurisdictional Wetland Dry During Release And Cleanup
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 368
Est Cost Prop Damage 0
Est Cost Emergency 93204
Est Cost Environmental 0
Est Cost Other 922664
Est Cost Other Details Cost To Investigate/locate Pinhole On Approx. 14 Miles Of Pipeline Segment.
Prpty 1016236
Accident Psig 1614
Mop Psig 1170
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Length Segment Isolated 47520
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Hydrostatic Pressure Test
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Ultrasonic Ind Yes
Geometry Deformation Ind Yes
Emat Ind Yes
Axial Recent Year 2006
Ultrasonic Recent Year 2008
Geometry Recent Year 2006
Emat Recent Year 2009
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2014
Hydrtst Most Rcnt Pressure 1614
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C**** K*******
Preparer Title Program Specialist
Preparer Email C*************@k***********.com
Preparer Telephone 316-828-4121
Preparer Fax 316-529-6377
Prepared Date 2015-09-21 00:00:00
Authorizer Name K** G*****
Authorizer Telephone 651-438-1775
Authorizer Title Dot Compliance Specialist
Authorizer Email K*********@k***********.com
Narrative On september 25, 2014 at 9:15 a.M., koch pipeline company ("kpl") located a small release on the minnesota pipe line 2 ("mpl 2") loop 7 pipeline segment from zimmerman to hugo, and more specifically located near milepost 218 during a hydrostatic test. At the time of the hydrostatic test, the line was not connected to the main pipeline and was being monitored locally and not by the pipeline control center. The location of the release was determined to be within a jurisdictional wetland, although at the time of the release the wetland was dry and no surface waters were impacted. Due to this area being a jurisdictional wetland, it is considered a release to surface water, but since the wetland was dry at the time, the only known impact was to soil. A metallurgical investigation of the pipe concluded that the cause of the test failure (near mp218) was a manufacturing defect, a through wall lack of fusion in the longitudinal seam. The failure occurred during the spike test, at pressure higher than the original pipe mill test pressure, with no indication of fatigue growth. Approximately 2,000 gallons of hydrostatic test water with a small amount of residual crude oil were released. Through third party sampling, it was estimated that 88-165 gallons of crude oil were released along with the hydrostatic test water. Upon discovery, the pipeline was immediately clamped to stop leakage, cleanup was initiated, and necessary repairs were undertaken. All contaminated soil was removed off site to be treated and clean backfill soil was replaced in the excavation. The total amount of soil remediated was approximately 915 tons.

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