HL incident on 2014-09-18 — TX

Operator
Enterprise Products Operating Llc
Cause
Notification Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$510,000
Incident datetime
2014-09-18 17:36
Report number
Location
TX
Narrative
On 9/18/2014 at 17:36 ct, enterprise pipeline control received a call from a farmer stating that he had hit a pipeline while plowing his field. The pipeline was not flowing at the time of the accident, and the impacted pipeline segment was isolated. Approximately 250 bbls of diesel leaked from the pipe. On 9/20/2014 a plidco sleeve was installed as a temporary repair and the pipeline was returned to service. The plicdo sleeve was replaced with a permanent repair on 9/22/2015 using 98ft of higher grade pipe (x52, 0.375wt) buried at a depth of 32 inches to avoid recurrence. All remediation has been completed. Nrc was notified when it was determined that costs exceeded the reporting threshold.
Detailed record list
Report Received Date
2014-10-17 00:00:00
Iyear
2014
Report Number
20140367
Supplemental Number
34354
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-09-18 17:36:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
250
Recovered Bbls
250
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2014-09-18 17:36:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Flowing At The Time Of The Accident.
On Site Datetime
2014-09-18 18:15:00
Nrc Rpt Datetime
2014-09-18 18:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
P74
Segment Name
Mcrae To West Memphis
Onshore State Abbreviation
Ar
Onshore Postal Code
72060
Onshore City Name
Griffithville
Onshore County Name
White
Designated Location
Milepost/valve Station
Designated Name
Mp8
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
7
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
Api-5l
Pipe Seam Type
Seamless
Pipe Manufacturer
National Tube
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
1954
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
2.5
Puncture Circum
1
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
31500
Est Cost Prop Damage
510000
Est Cost Emergency
200000
Est Cost Environmental
1000000
Est Cost Other
0
Prpty
1741500
Accident Psig
285
Mop Psig
1226
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
58080
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The line was not flowing at the time of the line strike.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Excavator Type
Farmer
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
No
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
H*** D***
Preparer Title
Sr. Pipeline Compliance Engineer
Preparer Email
H****@e****.com
Preparer Telephone
713-381-4277
Prepared Date
2020-10-08 00:00:00
Authorizer Name
H*** D***
Authorizer Telephone
713-381-4277
Authorizer Title
Sr. Pipeline Compliance Engineer
Authorizer Email
H****@e****.com
Narrative
On 9/18/2014 at 17:36 ct, enterprise pipeline control received a call from a farmer stating that he had hit a pipeline while plowing his field. The pipeline was not flowing at the time of the accident, and the impacted pipeline segment was isolated. Approximately 250 bbls of diesel leaked from the pipe. On 9/20/2014 a plidco sleeve was installed as a temporary repair and the pipeline was returned to service. The plicdo sleeve was replaced with a permanent repair on 9/22/2015 using 98ft of higher grade pipe (x52, 0.375wt) buried at a depth of 32 inches to avoid recurrence. All remediation has been completed. Nrc was notified when it was determined that costs exceeded the reporting threshold.
Report Received Date 2014-10-17 00:00:00
Iyear 2014
Report Number 20140367
Supplemental Number 34354
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-09-18 17:36:00
Location Latitude 35.13221 Google Maps OpenStreetMap
Location Longitude -91.59935 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 250
Recovered Bbls 250
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2014-09-18 17:36:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Not Flowing At The Time Of The Accident.
On Site Datetime 2014-09-18 18:15:00
Nrc Rpt Datetime 2014-09-18 18:45:00
Nrc Rpt Num 1095782 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name P74
Segment Name Mcrae To West Memphis
Onshore State Abbreviation Ar
Onshore Postal Code 72060
Onshore City Name Griffithville
Onshore County Name White
Designated Location Milepost/valve Station
Designated Name Mp8
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 7
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification Api-5l
Pipe Seam Type Seamless
Pipe Manufacturer National Tube
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year 1954
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 2.5
Puncture Circum 1
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 31500
Est Cost Prop Damage 510000
Est Cost Emergency 200000
Est Cost Environmental 1000000
Est Cost Other 0
Prpty 1741500
Accident Psig 285
Mop Psig 1226
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 58080
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The line was not flowing at the time of the line strike.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Pipeline Easement Row Ind Yes
Excavator Type Farmer
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks Unknown/other
Service Interruption No
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name H*** D***
Preparer Title Sr. Pipeline Compliance Engineer
Preparer Email H****@e****.com
Preparer Telephone 713-381-4277
Prepared Date 2020-10-08 00:00:00
Authorizer Name H*** D***
Authorizer Telephone 713-381-4277
Authorizer Title Sr. Pipeline Compliance Engineer
Authorizer Email H****@e****.com
Narrative On 9/18/2014 at 17:36 ct, enterprise pipeline control received a call from a farmer stating that he had hit a pipeline while plowing his field. The pipeline was not flowing at the time of the accident, and the impacted pipeline segment was isolated. Approximately 250 bbls of diesel leaked from the pipe. On 9/20/2014 a plidco sleeve was installed as a temporary repair and the pipeline was returned to service. The plicdo sleeve was replaced with a permanent repair on 9/22/2015 using 98ft of higher grade pipe (x52, 0.375wt) buried at a depth of 32 inches to avoid recurrence. All remediation has been completed. Nrc was notified when it was determined that costs exceeded the reporting threshold.

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