HL incident on 2014-09-01 — TX

Operator
Fieldwood Energy, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250,000
Incident datetime
2014-09-01 08:00
Report number
Location
TX
Narrative
Site personnel discovered oil on ground above buried pipeline section within site berm. Pipeline and facility shut down as a precaution. Excavation revealed additional oil below ground. Further investigation revealed a pinhole leak in the buried pipeline segment and numerous leaks from nearby threaded drain lines (not connected to pipeline) that contributed to the oil leakage. Note that the amount of oil spilled / recovered is not all associated with the leak on the DOT pipeline, but includes numerous leaks from other buried site piping. Much of the uncovered piping appears to be original to this site. This facility was placed in operation in or about 1965. The decision was made by fieldwood management to proactively replace the entire buried section of pipeline and move this segment and all other active piping, above ground. Review of the failed section of pipeline revealed a small pinhole leak in a 45 deg fitting, downstream of a girth weld. Examination of internal and external pipe surfaces revealed no evidence of corrosion or other damage in the area of failure.
Detailed record list
Report Received Date
2014-10-07 00:00:00
Iyear
2014
Report Number
20140355
Supplemental Number
20453
Report Type
Supplemental Final
Operator Id
Name
Fieldwood Energy, Llc
Operator Street Address
2000 W. Sam Houston Pkwy South 1200
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2014-09-01 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
10
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-09-01 08:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-09-01 08:00:00
Restart Datetime
2014-09-17 08:00:00
On Site Datetime
2014-09-01 08:00:00
Nrc Rpt Datetime
2014-09-08 16:10:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Grand Isle Tank Battery
Segment Name
Gi 43 Pipeline / 9084
Onshore State Abbreviation
La
Onshore Postal Code
70358
Onshore City Name
Grand Isle
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
At The Gitb
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.5
Pipe Smys
42000
Pipe Specification
Api 5lx42
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1990
Manufactured Year
1990
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
4
Rel Water Name
Contained In Boat Slip
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
250000
Est Cost Emergency
0
Est Cost Environmental
1000000
Est Cost Other
0
Est Cost Other Details
No Estimated Other Cost
Prpty
1250000
Accident Psig
15
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
80
Internal Inspection Ind
No
Diameter Change Ind
Yes
Tight Mitered Ind
Yes
Other Restrictions Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Anomaly Cause During Manufacturing Or Fabrication Process
Pwf Additional Other Ind
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
B**** M*******
Preparer Title
Sems Coordinator
Preparer Email
B*************@f*****.com
Preparer Telephone
337-354-8118
Prepared Date
2015-05-18 00:00:00
Authorizer Name
B**** M*******
Authorizer Telephone
337-354-8118
Authorizer Title
Sems Coordinator
Authorizer Email
B*************@f*****.com
Narrative
Site personnel discovered oil on ground above buried pipeline section within site berm. Pipeline and facility shut down as a precaution. Excavation revealed additional oil below ground. Further investigation revealed a pinhole leak in the buried pipeline segment and numerous leaks from nearby threaded drain lines (not connected to pipeline) that contributed to the oil leakage. Note that the amount of oil spilled / recovered is not all associated with the leak on the DOT pipeline, but includes numerous leaks from other buried site piping. Much of the uncovered piping appears to be original to this site. This facility was placed in operation in or about 1965. The decision was made by fieldwood management to proactively replace the entire buried section of pipeline and move this segment and all other active piping, above ground. Review of the failed section of pipeline revealed a small pinhole leak in a 45 deg fitting, downstream of a girth weld. Examination of internal and external pipe surfaces revealed no evidence of corrosion or other damage in the area of failure.
Report Received Date 2014-10-07 00:00:00
Iyear 2014
Report Number 20140355
Supplemental Number 20453
Report Type Supplemental Final
Operator Id 39068 PHMSA Enforcement
Name Fieldwood Energy, Llc
Operator Street Address 2000 W. Sam Houston Pkwy South 1200
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2014-09-01 08:00:00
Location Latitude 29.25694 Google Maps OpenStreetMap
Location Longitude -89.96583 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 10
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-09-01 08:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-09-01 08:00:00
Restart Datetime 2014-09-17 08:00:00
On Site Datetime 2014-09-01 08:00:00
Nrc Rpt Datetime 2014-09-08 16:10:00
Nrc Rpt Num 1094400 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Grand Isle Tank Battery
Segment Name Gi 43 Pipeline / 9084
Onshore State Abbreviation La
Onshore Postal Code 70358
Onshore City Name Grand Isle
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name At The Gitb
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Pipe Wall Thickness 0.5
Pipe Smys 42000
Pipe Specification Api 5lx42
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 1990
Manufactured Year 1990
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 4
Rel Water Name Contained In Boat Slip
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 250000
Est Cost Emergency 0
Est Cost Environmental 1000000
Est Cost Other 0
Est Cost Other Details No Estimated Other Cost
Prpty 1250000
Accident Psig 15
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 80
Internal Inspection Ind No
Diameter Change Ind Yes
Tight Mitered Ind Yes
Other Restrictions Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Anomaly Cause During Manufacturing Or Fabrication Process
Pwf Additional Other Ind Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name B**** M*******
Preparer Title Sems Coordinator
Preparer Email B*************@f*****.com
Preparer Telephone 337-354-8118
Prepared Date 2015-05-18 00:00:00
Authorizer Name B**** M*******
Authorizer Telephone 337-354-8118
Authorizer Title Sems Coordinator
Authorizer Email B*************@f*****.com
Narrative Site personnel discovered oil on ground above buried pipeline section within site berm. Pipeline and facility shut down as a precaution. Excavation revealed additional oil below ground. Further investigation revealed a pinhole leak in the buried pipeline segment and numerous leaks from nearby threaded drain lines (not connected to pipeline) that contributed to the oil leakage. Note that the amount of oil spilled / recovered is not all associated with the leak on the DOT pipeline, but includes numerous leaks from other buried site piping. Much of the uncovered piping appears to be original to this site. This facility was placed in operation in or about 1965. The decision was made by fieldwood management to proactively replace the entire buried section of pipeline and move this segment and all other active piping, above ground. Review of the failed section of pipeline revealed a small pinhole leak in a 45 deg fitting, downstream of a girth weld. Examination of internal and external pipe surfaces revealed no evidence of corrosion or other damage in the area of failure.

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