HL incident on 2014-09-05 — WY

Operator
Belle Fourche Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2014-09-05 20:30
Report number
Location
WY
Narrative
Both incoming belle fourche pipeline valves closed at the same time for a brief time causing a pressure spike. The low pressure, 250 psi, relief designed to relief at 275 psi failed to open which allowed over pressuring of the meter causing one of the meter gaskets to fail. A belle fourche pipeline employee was on scene and was able to isolate the failed gasket. The meter was removed from the line following the incident and put out of service until a rebuild kit has been installed.
Detailed record list
Report Received Date
2014-10-03 00:00:00
Iyear
2014
Report Number
20140351
Supplemental Number
19771
Report Type
Original Final
Operator Id
Name
Belle Fourche Pipeline Co
Operator Street Address
455 N Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Local Datetime
2014-09-05 20:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
10
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-09-05 20:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2014-09-05 20:30:00
Ignite Ind
No
Explode Ind
No
Onshore State Abbreviation
Wy
Onshore Postal Code
82214
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Material Involved
Material Other Than Carbon Steel
Material Details
Gerlock Gasket
Release Type
Leak
Leak Type
Seal Or Packing
Leak Type Other
Gasket Failure
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
2000
Est Cost Other
0
Prpty
4000
Accident Psig
420
Mop Psig
275
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Other Control Relief Ind
Yes
Other Control Relief Details
Meter
Additional Overpressure Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Low Pressure Pop Off Failure
Preparer Name
J**** C* R*********
Preparer Title
Dot Compliance Coodinator
Preparer Email
J***************@t******.com
Preparer Telephone
3072660250
Prepared Date
2014-09-25 00:00:00
Authorizer Name
J**** C* R*********
Authorizer Telephone
3072660250
Authorizer Email
No Email Address
Narrative
Both incoming belle fourche pipeline valves closed at the same time for a brief time causing a pressure spike. The low pressure, 250 psi, relief designed to relief at 275 psi failed to open which allowed over pressuring of the meter causing one of the meter gaskets to fail. A belle fourche pipeline employee was on scene and was able to isolate the failed gasket. The meter was removed from the line following the incident and put out of service until a rebuild kit has been installed.
Report Received Date 2014-10-03 00:00:00
Iyear 2014
Report Number 20140351
Supplemental Number 19771
Report Type Original Final
Operator Id 1248 PHMSA Enforcement
Name Belle Fourche Pipeline Co
Operator Street Address 455 N Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82602
Local Datetime 2014-09-05 20:30:00
Location Latitude 42.225543 Google Maps OpenStreetMap
Location Longitude -104.694563 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 10
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-09-05 20:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
On Site Datetime 2014-09-05 20:30:00
Ignite Ind No
Explode Ind No
Onshore State Abbreviation Wy
Onshore Postal Code 82214
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Material Involved Material Other Than Carbon Steel
Material Details Gerlock Gasket
Release Type Leak
Leak Type Seal Or Packing
Leak Type Other Gasket Failure
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 2000
Est Cost Other 0
Prpty 4000
Accident Psig 420
Mop Psig 275
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Other Control Relief Ind Yes
Other Control Relief Details Meter
Additional Overpressure Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Low Pressure Pop Off Failure
Preparer Name J**** C* R*********
Preparer Title Dot Compliance Coodinator
Preparer Email J***************@t******.com
Preparer Telephone 3072660250
Prepared Date 2014-09-25 00:00:00
Authorizer Name J**** C* R*********
Authorizer Telephone 3072660250
Authorizer Email No Email Address
Narrative Both incoming belle fourche pipeline valves closed at the same time for a brief time causing a pressure spike. The low pressure, 250 psi, relief designed to relief at 275 psi failed to open which allowed over pressuring of the meter causing one of the meter gaskets to fail. A belle fourche pipeline employee was on scene and was able to isolate the failed gasket. The meter was removed from the line following the incident and put out of service until a rebuild kit has been installed.

All rights reserved. Copyright © by ClearPHMSA