HL incident on 2014-09-17 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2014-09-17 12:55
Report number
Location
TX
Narrative
12:55 a report of gasoline ordor at valve box #6 by field personnel. 15:15 field reoprted that a vac truck was in route. Found about 4'' of product in the 6x6 valve box. 19:20 vault clean out ... Line restarted to inspect the piping in the vault. A small leak was discoverd at the bottom of the mainline block valve cavity relief valve. Relief valve replaced, line restarted to reinspect the valve. All ok. 19:30 stand up pressure test np01. 20:30 pressure test ended, given ok to return line to normal operation. 21:35 line up and runing.
Detailed record list
Report Received Date
2014-10-02 00:00:00
Iyear
2014
Report Number
20140349
Supplemental Number
19815
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2014-09-17 12:55:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
2.13
Recovered Bbls
2.13
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-09-17 12:55:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-09-17 12:55:00
Restart Datetime
2014-09-17 19:35:00
On Site Datetime
2014-09-17 12:55:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Richmond Products Line
Segment Name
Np-01
Onshore State Abbreviation
Ca
Onshore Postal Code
94806
Onshore City Name
Richmond
Onshore County Name
Contra Costa
Designated Location
Milepost/valve Station
Designated Name
Valve Site #6
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
500
Est Cost Emergency
4300
Est Cost Environmental
0
Est Cost Other
0
Prpty
5000
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
B**** G****
Preparer Title
Dot Coordinator
Preparer Email
B**********@p**.com
Preparer Telephone
9092413358
Preparer Fax
5622901580
Prepared Date
2014-10-23 00:00:00
Authorizer Name
T*** T*****
Authorizer Telephone
8327651636
Authorizer Title
Manager Regulatory Compliance
Authorizer Email
T************@p**.com
Narrative
12:55 a report of gasoline ordor at valve box #6 by field personnel. 15:15 field reoprted that a vac truck was in route. Found about 4'' of product in the 6x6 valve box. 19:20 vault clean out ... Line restarted to inspect the piping in the vault. A small leak was discoverd at the bottom of the mainline block valve cavity relief valve. Relief valve replaced, line restarted to reinspect the valve. All ok. 19:30 stand up pressure test np01. 20:30 pressure test ended, given ok to return line to normal operation. 21:35 line up and runing.
Report Received Date 2014-10-02 00:00:00
Iyear 2014
Report Number 20140349
Supplemental Number 19815
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2014-09-17 12:55:00
Location Latitude 37.976654 Google Maps OpenStreetMap
Location Longitude -122.322127 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 2.13
Recovered Bbls 2.13
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-09-17 12:55:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-09-17 12:55:00
Restart Datetime 2014-09-17 19:35:00
On Site Datetime 2014-09-17 12:55:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Richmond Products Line
Segment Name Np-01
Onshore State Abbreviation Ca
Onshore Postal Code 94806
Onshore City Name Richmond
Onshore County Name Contra Costa
Designated Location Milepost/valve Station
Designated Name Valve Site #6
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 500
Est Cost Emergency 4300
Est Cost Environmental 0
Est Cost Other 0
Prpty 5000
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Preparer Name B**** G****
Preparer Title Dot Coordinator
Preparer Email B**********@p**.com
Preparer Telephone 9092413358
Preparer Fax 5622901580
Prepared Date 2014-10-23 00:00:00
Authorizer Name T*** T*****
Authorizer Telephone 8327651636
Authorizer Title Manager Regulatory Compliance
Authorizer Email T************@p**.com
Narrative 12:55 a report of gasoline ordor at valve box #6 by field personnel. 15:15 field reoprted that a vac truck was in route. Found about 4'' of product in the 6x6 valve box. 19:20 vault clean out ... Line restarted to inspect the piping in the vault. A small leak was discoverd at the bottom of the mainline block valve cavity relief valve. Relief valve replaced, line restarted to reinspect the valve. All ok. 19:30 stand up pressure test np01. 20:30 pressure test ended, given ok to return line to normal operation. 21:35 line up and runing.

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