HL incident on 2014-09-01 — WY

Operator
Butte Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2014-09-01 12:00
Report number
Location
WY
Narrative
The 500t valve was opened which allowed crude to flow to the globe valve designed to control downstream pressure to the meter run and tank. Due to manufacturing defect the packing on the globe valve failed causing a leak. The globe valve that was leaking was replaced and the line was returned to service.
Detailed record list
Report Received Date
2014-09-30 00:00:00
Iyear
2014
Report Number
20140345
Supplemental Number
19762
Report Type
Original Final
Operator Id
Name
Butte Pipeline Co
Operator Street Address
455 N. Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82601
Local Datetime
2014-09-01 08:00:00
Location Latitude
Location Longitude
-104.7148125
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-09-01 12:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-09-01 12:00:00
Restart Datetime
2014-09-23 13:00:00
On Site Datetime
2014-09-01 12:00:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Onshore State Abbreviation
Mt
Onshore Postal Code
59311
Federal
Yes
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
350
Est Cost Prop Damage
5000
Est Cost Emergency
0
Est Cost Environmental
3000
Est Cost Other
0
Prpty
8350
Accident Psig
180
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
170
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Station Piping Including Meter.
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The mop was not exceeded in the incident. The globe valve failed due to manufacture defect with the packing.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Control Valve Ind
Yes
Additional Defect Ind
Yes
Preparer Name
J**** C* R*********
Preparer Title
Dot Compliance Cordinator
Preparer Email
J***************@t******.com
Preparer Telephone
3072660250
Prepared Date
2014-09-30 00:00:00
Authorizer Name
J**** C* R*********
Authorizer Telephone
3072660250
Authorizer Email
No Email Address
Narrative
The 500t valve was opened which allowed crude to flow to the globe valve designed to control downstream pressure to the meter run and tank. Due to manufacturing defect the packing on the globe valve failed causing a leak. The globe valve that was leaking was replaced and the line was returned to service.
Report Received Date 2014-09-30 00:00:00
Iyear 2014
Report Number 20140345
Supplemental Number 19762
Report Type Original Final
Operator Id 1960 PHMSA Enforcement
Name Butte Pipeline Co
Operator Street Address 455 N. Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82601
Local Datetime 2014-09-01 08:00:00
Location Latitude 45.15209388 Google Maps OpenStreetMap
Location Longitude -104.7148125 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-09-01 12:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-09-01 12:00:00
Restart Datetime 2014-09-23 13:00:00
On Site Datetime 2014-09-01 12:00:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Onshore State Abbreviation Mt
Onshore Postal Code 59311
Federal Yes
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 350
Est Cost Prop Damage 5000
Est Cost Emergency 0
Est Cost Environmental 3000
Est Cost Other 0
Prpty 8350
Accident Psig 180
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 170
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Station Piping Including Meter.
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The mop was not exceeded in the incident. The globe valve failed due to manufacture defect with the packing.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Control Valve Ind Yes
Additional Defect Ind Yes
Preparer Name J**** C* R*********
Preparer Title Dot Compliance Cordinator
Preparer Email J***************@t******.com
Preparer Telephone 3072660250
Prepared Date 2014-09-30 00:00:00
Authorizer Name J**** C* R*********
Authorizer Telephone 3072660250
Authorizer Email No Email Address
Narrative The 500t valve was opened which allowed crude to flow to the globe valve designed to control downstream pressure to the meter run and tank. Due to manufacturing defect the packing on the globe valve failed causing a leak. The globe valve that was leaking was replaced and the line was returned to service.

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