HL incident on 2014-08-25 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2014-08-25 21:00
Report number
Location
OK
Narrative
During a delivery of 14# natural gasoline the outboard seal on pump #3 failed, causing a release. Tulsa pipeline control center received a float seal fail alarm and pump shutdown automatically. Mechanic had replaced seals on pump #3 on 8/13/2104. Investigation determined that during the replacement on 8/13/14 mechanic failed to properly tighten the seal retaining bolts. Between 8/13/2014 and the release on 8/25/14 the pump had approximately 16 hours of run time. Supervisor and mechanics reviewed the procedure to ensure it was effective and no changes were identified. Mechanic was retrained on procedure.
Detailed record list
Report Received Date
2014-09-19 00:00:00
Iyear
2014
Report Number
20140332
Supplemental Number
20396
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-08-25 21:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
52
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-08-25 21:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-08-25 21:00:00
Restart Datetime
2014-08-26 09:00:00
On Site Datetime
2014-08-25 21:03:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Medford North Line #2 Pump Header
Segment Name
Index 10129
Onshore State Abbreviation
Ok
Onshore Postal Code
73759
Onshore City Name
Medford
Onshore County Name
Grant
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Seal Material
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
331
Est Cost Prop Damage
3000
Est Cost Emergency
2500
Est Cost Environmental
1000
Est Cost Other
0
Prpty
6831
Accident Psig
1200
Mop Psig
1800
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller had not made any changes to operation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2015-04-29 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
During a delivery of 14# natural gasoline the outboard seal on pump #3 failed, causing a release. Tulsa pipeline control center received a float seal fail alarm and pump shutdown automatically. Mechanic had replaced seals on pump #3 on 8/13/2104. Investigation determined that during the replacement on 8/13/14 mechanic failed to properly tighten the seal retaining bolts. Between 8/13/2014 and the release on 8/25/14 the pump had approximately 16 hours of run time. Supervisor and mechanics reviewed the procedure to ensure it was effective and no changes were identified. Mechanic was retrained on procedure.
Report Received Date 2014-09-19 00:00:00
Iyear 2014
Report Number 20140332
Supplemental Number 20396
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2014-08-25 21:00:00
Location Latitude 36.773611 Google Maps OpenStreetMap
Location Longitude -97.756389 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 52
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2014-08-25 21:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-08-25 21:00:00
Restart Datetime 2014-08-26 09:00:00
On Site Datetime 2014-08-25 21:03:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Medford North Line #2 Pump Header
Segment Name Index 10129
Onshore State Abbreviation Ok
Onshore Postal Code 73759
Onshore City Name Medford
Onshore County Name Grant
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Seal Material
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 331
Est Cost Prop Damage 3000
Est Cost Emergency 2500
Est Cost Environmental 1000
Est Cost Other 0
Prpty 6831
Accident Psig 1200
Mop Psig 1800
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller had not made any changes to operation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind No
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2015-04-29 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative During a delivery of 14# natural gasoline the outboard seal on pump #3 failed, causing a release. Tulsa pipeline control center received a float seal fail alarm and pump shutdown automatically. Mechanic had replaced seals on pump #3 on 8/13/2104. Investigation determined that during the replacement on 8/13/14 mechanic failed to properly tighten the seal retaining bolts. Between 8/13/2014 and the release on 8/25/14 the pump had approximately 16 hours of run time. Supervisor and mechanics reviewed the procedure to ensure it was effective and no changes were identified. Mechanic was retrained on procedure.

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