HL incident on 2014-08-21 — TX

Operator
Plantation Pipe Line Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$600,000
Incident datetime
2014-08-21 16:30
Report number
Location
TX
Narrative
A resident called the control center at 15:42 on 8/21/2014 to report product near the right of way. Once the leak site was discovered and the pipeline excavated, a field examination determined the longitudinal weld of a type "b" sleev had a crack. The type "b" sleeve was installed in 1979 to repair a dent in the pipeline discovered from a kaliper pig survey. The location of the product release was a dent centered at the 6:00 circumferential position in nps 30 linepipe that was sleeved in 1979. Metallurgical analysis indicates the leak path involved a 2 3/8 inch longitudinal crack in the shoulder of the dent at the 5:30 circumferential position and an 83/4-inch long crack in the sleeve longitudinal weld at the 3:00 circumferential position. The longitudinal edges of the both sleeve pieces were somewhat flat rather than fully contoured to the outside diameter of the linepipe. This created peaking conditions at both longitudinal weld seams in the sleeve. The longitudinal seam weld at 3:00 that leaked also exhibited a wide root gap and the backing strip beneath the sleeve did not extend fully across the gap. The result of the fit-up was a weld with incomplete penetration and non-fusion along the edges of the root, particularly along the edge that lacked backing. The most likely sequence of events is that the dent leaked first. After the dent subsequently leaked and pressurized the sleeve, the cap pass of the longitudinal sleeve weld could not support the load and fractured by tensile overload. Residual impacts are being addressed under the oversight of the alabama department of environmental management, groundwater section.
Detailed record list
Report Received Date
2014-09-18 00:00:00
Iyear
2014
Report Number
20140330
Supplemental Number
30984
Report Type
Supplemental Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana Street, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-08-21 15:42:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
919
Recovered Bbls
338
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2014-08-21 16:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-08-21 15:44:00
Restart Datetime
2014-08-25 12:53:00
On Site Datetime
2014-08-21 16:30:00
Nrc Rpt Datetime
2014-08-21 21:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
30 Inch Cng Pipeline
Segment Name
Line Section 4b
Onshore State Abbreviation
Al
Onshore Postal Code
35124
Onshore City Name
Pelham
Onshore County Name
Shelby
Designated Location
Milepost/valve Station
Designated Name
331
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
120
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Other Butt Weld
Installation Year
1979
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0
Rel Water Name
Unknown
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
64000
Est Cost Prop Damage
600000
Est Cost Emergency
2830000
Est Cost Environmental
5000000
Est Cost Other
0
Prpty
8494000
Accident Psig
196
Mop Psig
779
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
312840
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind
Yes
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
B Sleeve Weld Had Incomplete Penetration And Non Fusion Along Edges Of The Root.
Additional Crack Ind
Yes
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2013
Geometry Recent Year
2013
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Q****** H* F******
Preparer Title
Manager-Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-741-4240
Preparer Fax
770-751-4130
Prepared Date
2018-09-27 00:00:00
Authorizer Name
Q****** H* F******
Authorizer Telephone
770-751-4240
Authorizer Title
Manager-Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
A resident called the control center at 15:42 on 8/21/2014 to report product near the right of way. Once the leak site was discovered and the pipeline excavated, a field examination determined the longitudinal weld of a type "b" sleev had a crack. The type "b" sleeve was installed in 1979 to repair a dent in the pipeline discovered from a kaliper pig survey. The location of the product release was a dent centered at the 6:00 circumferential position in nps 30 linepipe that was sleeved in 1979. Metallurgical analysis indicates the leak path involved a 2 3/8 inch longitudinal crack in the shoulder of the dent at the 5:30 circumferential position and an 83/4-inch long crack in the sleeve longitudinal weld at the 3:00 circumferential position. The longitudinal edges of the both sleeve pieces were somewhat flat rather than fully contoured to the outside diameter of the linepipe. This created peaking conditions at both longitudinal weld seams in the sleeve. The longitudinal seam weld at 3:00 that leaked also exhibited a wide root gap and the backing strip beneath the sleeve did not extend fully across the gap. The result of the fit-up was a weld with incomplete penetration and non-fusion along the edges of the root, particularly along the edge that lacked backing. The most likely sequence of events is that the dent leaked first. After the dent subsequently leaked and pressurized the sleeve, the cap pass of the longitudinal sleeve weld could not support the load and fractured by tensile overload. Residual impacts are being addressed under the oversight of the alabama department of environmental management, groundwater section.
Report Received Date 2014-09-18 00:00:00
Iyear 2014
Report Number 20140330
Supplemental Number 30984
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana Street, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-08-21 15:42:00
Location Latitude 33.286639 Google Maps OpenStreetMap
Location Longitude -86.74691 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 919
Recovered Bbls 338
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2014-08-21 16:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-08-21 15:44:00
Restart Datetime 2014-08-25 12:53:00
On Site Datetime 2014-08-21 16:30:00
Nrc Rpt Datetime 2014-08-21 21:05:00
Nrc Rpt Num 1093064 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name 30 Inch Cng Pipeline
Segment Name Line Section 4b
Onshore State Abbreviation Al
Onshore Postal Code 35124
Onshore City Name Pelham
Onshore County Name Shelby
Designated Location Milepost/valve Station
Designated Name 331
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 120
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Other Butt Weld
Installation Year 1979
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0
Rel Water Name Unknown
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 64000
Est Cost Prop Damage 600000
Est Cost Emergency 2830000
Est Cost Environmental 5000000
Est Cost Other 0
Prpty 8494000
Accident Psig 196
Mop Psig 779
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 312840
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Field Exam Ind Yes
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details B Sleeve Weld Had Incomplete Penetration And Non Fusion Along Edges Of The Root.
Additional Crack Ind Yes
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2013
Geometry Recent Year 2013
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name Q****** H* F******
Preparer Title Manager-Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-741-4240
Preparer Fax 770-751-4130
Prepared Date 2018-09-27 00:00:00
Authorizer Name Q****** H* F******
Authorizer Telephone 770-751-4240
Authorizer Title Manager-Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative A resident called the control center at 15:42 on 8/21/2014 to report product near the right of way. Once the leak site was discovered and the pipeline excavated, a field examination determined the longitudinal weld of a type "b" sleev had a crack. The type "b" sleeve was installed in 1979 to repair a dent in the pipeline discovered from a kaliper pig survey. The location of the product release was a dent centered at the 6:00 circumferential position in nps 30 linepipe that was sleeved in 1979. Metallurgical analysis indicates the leak path involved a 2 3/8 inch longitudinal crack in the shoulder of the dent at the 5:30 circumferential position and an 83/4-inch long crack in the sleeve longitudinal weld at the 3:00 circumferential position. The longitudinal edges of the both sleeve pieces were somewhat flat rather than fully contoured to the outside diameter of the linepipe. This created peaking conditions at both longitudinal weld seams in the sleeve. The longitudinal seam weld at 3:00 that leaked also exhibited a wide root gap and the backing strip beneath the sleeve did not extend fully across the gap. The result of the fit-up was a weld with incomplete penetration and non-fusion along the edges of the root, particularly along the edge that lacked backing. The most likely sequence of events is that the dent leaked first. After the dent subsequently leaked and pressurized the sleeve, the cap pass of the longitudinal sleeve weld could not support the load and fractured by tensile overload. Residual impacts are being addressed under the oversight of the alabama department of environmental management, groundwater section.

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