HL incident on 2014-08-19 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2014-08-19 10:00
Report number
Location
TX
Narrative
On 8/19/2014, local operating personnel noticed an accumulation of product near the millennium scraper trap enclosure. Investigation determined that the o-ring seal on the enclosure was leaking due to wear. The line was shut down. The o-ring was removed and a new o-ring was installed. The line was restarted and the trap enclosure was monitored with no evidence of leakage following the o-ring replacement. Free product was removed via vacuum truck and the affected area was cleaned.
Detailed record list
Report Received Date
2014-09-17 00:00:00
Iyear
2014
Report Number
20140326
Supplemental Number
19731
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-08-19 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-08-19 10:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-08-19 10:00:00
Restart Datetime
2014-08-19 10:30:00
On Site Datetime
2014-08-19 10:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Nederland To Longview 12"
Segment Name
21010-12" Nederland To Longview
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
1+90.7
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
71
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
500
Est Cost Other
0
Prpty
671
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2014-09-17 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 8/19/2014, local operating personnel noticed an accumulation of product near the millennium scraper trap enclosure. Investigation determined that the o-ring seal on the enclosure was leaking due to wear. The line was shut down. The o-ring was removed and a new o-ring was installed. The line was restarted and the trap enclosure was monitored with no evidence of leakage following the o-ring replacement. Free product was removed via vacuum truck and the affected area was cleaned.
Report Received Date 2014-09-17 00:00:00
Iyear 2014
Report Number 20140326
Supplemental Number 19731
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-08-19 10:00:00
Location Latitude 29.99447 Google Maps OpenStreetMap
Location Longitude -93.99172 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.71
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-08-19 10:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-08-19 10:00:00
Restart Datetime 2014-08-19 10:30:00
On Site Datetime 2014-08-19 10:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Nederland To Longview 12"
Segment Name 21010-12" Nederland To Longview
Onshore State Abbreviation Tx
Onshore Postal Code 77627
Onshore City Name Nederland
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 1+90.7
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 71
Est Cost Prop Damage 100
Est Cost Emergency 0
Est Cost Environmental 500
Est Cost Other 0
Prpty 671
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2014-09-17 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 8/19/2014, local operating personnel noticed an accumulation of product near the millennium scraper trap enclosure. Investigation determined that the o-ring seal on the enclosure was leaking due to wear. The line was shut down. The o-ring was removed and a new o-ring was installed. The line was restarted and the trap enclosure was monitored with no evidence of leakage following the o-ring replacement. Free product was removed via vacuum truck and the affected area was cleaned.

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