HL incident on 2014-08-06 — TX

Operator
North Dakota Pipeline Company Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-08-06 14:02
Report number
Location
TX
Narrative
An explosion/fire occurred at the alexander station resulting in a release of approximately 2 gallons of crude oil (9 total gallons reported includes 7 additional gallons of drain down) and causing an injury to a contract employee. The incident occurred when welders were welding on a flange and a foreman's plug blew. A metallurgical analysis was conducted and confirmed porosity as a manufacturing defect. The analysis concluded that the flame from welding ignited vapors that had leaked through the large porosity holes in the foreman plug, the flames traveled back through the plug igniting vapors in the pipe which caused the plug to be ejected. The third party contractor was taken to a medical facility for treatment. Contractor was treated and released. 10/07/2016 in discussions with the plug's manufacturer following this incident, ndpl discovered that the manufacturer revised its specifications regarding use of the foremen's plug after ndpl's regular annual review of manufacturer's specifications in november 2013, and prior to ndpl's regularly scheduled annual review of said specifications in november 2014, recommending against use in this application. Ndpl maintains the porosity (manufacturing defect) discovered during the investigation of this incident was the root cause of the incident. Ndpl has agreed to update the 7000-1 from equipment failure to incorrect equipment after review with PHMSA accident investigator. Based on the change to the manufacturer's instruction, ndpl has revised its procedure and no longer includes the use of a foremen's plug in this application.
Detailed record list
Report Received Date
2014-09-05 00:00:00
Iyear
2014
Report Number
20140318
Supplemental Number
21848
Report Type
Supplemental Final
Operator Id
Name
North Dakota Pipeline Company Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2014-08-06 14:02:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.21
Recovered Bbls
0.21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-08-06 14:02:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Facility Was Shutdown Prior To Incident For Work Being Completed
On Site Datetime
2014-08-06 14:02:00
Nrc Rpt Datetime
2014-08-06 15:24:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
0
Pipe Fac Name
Alexander Station
Segment Name
Ax
Onshore State Abbreviation
Nd
Onshore Postal Code
58831
Onshore City Name
Alexander
Onshore County Name
Mckenzie
Designated Location
Milepost/valve Station
Designated Name
Ax Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Foreman Plug
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Alumimum Plug With Rubber Seal
Release Type
Leak
Leak Type
Other
Leak Type Other
Plug Ejected From Pipe
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
59207
Est Cost Environmental
0
Est Cost Other
14765
Est Cost Other Details
Misc., Food/lodging, Metalurgical Analysis ($6,000)
Prpty
73972
Accident Psig
0
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
No
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The nature of the release was related to construction activities on site
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
10
Num Employees Failed
0
Num Contractors Tested
12
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Other Ind
Yes
Operation Related Details
Device Used Per Industry Practice, Not Recommended For Use For This Application By Manufacturer. (See Narrative In Part H)
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
D**** S*****
Preparer Title
Compliance Team Lead
Preparer Email
D***********@e*******.com
Preparer Telephone
701-857-0815
Preparer Fax
701-857-0809
Prepared Date
2016-11-16 00:00:00
Authorizer Name
K**** G****
Authorizer Telephone
701-857-0880
Authorizer Title
Manager Support Services
Authorizer Email
K**********@e*******.com
Narrative
An explosion/fire occurred at the alexander station resulting in a release of approximately 2 gallons of crude oil (9 total gallons reported includes 7 additional gallons of drain down) and causing an injury to a contract employee. The incident occurred when welders were welding on a flange and a foreman's plug blew. A metallurgical analysis was conducted and confirmed porosity as a manufacturing defect. The analysis concluded that the flame from welding ignited vapors that had leaked through the large porosity holes in the foreman plug, the flames traveled back through the plug igniting vapors in the pipe which caused the plug to be ejected. The third party contractor was taken to a medical facility for treatment. Contractor was treated and released. 10/07/2016 in discussions with the plug's manufacturer following this incident, ndpl discovered that the manufacturer revised its specifications regarding use of the foremen's plug after ndpl's regular annual review of manufacturer's specifications in november 2013, and prior to ndpl's regularly scheduled annual review of said specifications in november 2014, recommending against use in this application. Ndpl maintains the porosity (manufacturing defect) discovered during the investigation of this incident was the root cause of the incident. Ndpl has agreed to update the 7000-1 from equipment failure to incorrect equipment after review with PHMSA accident investigator. Based on the change to the manufacturer's instruction, ndpl has revised its procedure and no longer includes the use of a foremen's plug in this application.
Report Received Date 2014-09-05 00:00:00
Iyear 2014
Report Number 20140318
Supplemental Number 21848
Report Type Supplemental Final
Operator Id 15774 PHMSA Enforcement
Name North Dakota Pipeline Company Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2014-08-06 14:02:00
Location Latitude 47.97958 Google Maps OpenStreetMap
Location Longitude -103.6615 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.21
Recovered Bbls 0.21
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-08-06 14:02:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Facility Was Shutdown Prior To Incident For Work Being Completed
On Site Datetime 2014-08-06 14:02:00
Nrc Rpt Datetime 2014-08-06 15:24:00
Nrc Rpt Num 1091521 NRC Report How to search
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 0
Pipe Fac Name Alexander Station
Segment Name Ax
Onshore State Abbreviation Nd
Onshore Postal Code 58831
Onshore City Name Alexander
Onshore County Name Mckenzie
Designated Location Milepost/valve Station
Designated Name Ax Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Foreman Plug
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Alumimum Plug With Rubber Seal
Release Type Leak
Leak Type Other
Leak Type Other Plug Ejected From Pipe
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 59207
Est Cost Environmental 0
Est Cost Other 14765
Est Cost Other Details Misc., Food/lodging, Metalurgical Analysis ($6,000)
Prpty 73972
Accident Psig 0
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind No
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The nature of the release was related to construction activities on site
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 10
Num Employees Failed 0
Num Contractors Tested 12
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Wrong Equipment Specified Or Installed
Operation Type Wrong Equipment Specified Or Installed
Related Other Ind Yes
Operation Related Details Device Used Per Industry Practice, Not Recommended For Use For This Application By Manufacturer. (See Narrative In Part H)
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name D**** S*****
Preparer Title Compliance Team Lead
Preparer Email D***********@e*******.com
Preparer Telephone 701-857-0815
Preparer Fax 701-857-0809
Prepared Date 2016-11-16 00:00:00
Authorizer Name K**** G****
Authorizer Telephone 701-857-0880
Authorizer Title Manager Support Services
Authorizer Email K**********@e*******.com
Narrative An explosion/fire occurred at the alexander station resulting in a release of approximately 2 gallons of crude oil (9 total gallons reported includes 7 additional gallons of drain down) and causing an injury to a contract employee. The incident occurred when welders were welding on a flange and a foreman's plug blew. A metallurgical analysis was conducted and confirmed porosity as a manufacturing defect. The analysis concluded that the flame from welding ignited vapors that had leaked through the large porosity holes in the foreman plug, the flames traveled back through the plug igniting vapors in the pipe which caused the plug to be ejected. The third party contractor was taken to a medical facility for treatment. Contractor was treated and released. 10/07/2016 in discussions with the plug's manufacturer following this incident, ndpl discovered that the manufacturer revised its specifications regarding use of the foremen's plug after ndpl's regular annual review of manufacturer's specifications in november 2013, and prior to ndpl's regularly scheduled annual review of said specifications in november 2014, recommending against use in this application. Ndpl maintains the porosity (manufacturing defect) discovered during the investigation of this incident was the root cause of the incident. Ndpl has agreed to update the 7000-1 from equipment failure to incorrect equipment after review with PHMSA accident investigator. Based on the change to the manufacturer's instruction, ndpl has revised its procedure and no longer includes the use of a foremen's plug in this application.

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