HL incident on 2014-08-02 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2014-08-02 11:40
Report number
Location
OK
Narrative
Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated.
Detailed record list
Report Received Date
2014-09-02 00:00:00
Iyear
2014
Report Number
20140311
Supplemental Number
20753
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-08-02 11:40:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
10
Recovered Bbls
3.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2014-08-02 11:40:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Product Transferred To Another Tank. Pipeline Was Not Active At The Time
On Site Datetime
2014-08-02 11:40:00
Nrc Rpt Datetime
2014-08-02 15:09:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Chicago Terminal #206
Segment Name
Tank #715
Onshore State Abbreviation
Il
Onshore Postal Code
60131
Onshore City Name
Franklin Park
Onshore County Name
Cook
Designated Location
Milepost/valve Station
Designated Name
304.58
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Api Std Out Of Service Year
1998
Api Std In Service Year
2010
Installation Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
25000
Est Cost Emergency
10000
Est Cost Environmental
60000
Est Cost Other
0
Prpty
96000
Accident Psig
9
Mop Psig
13
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was caused by corrosion in the tank floor. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Localized Coating Failure
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Area Of Coating Failure
Corrosion Inhibitors
No
Corrosion Lining
Yes
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7337
Prepared Date
2015-09-18 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated.
Report Received Date 2014-09-02 00:00:00
Iyear 2014
Report Number 20140311
Supplemental Number 20753
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2014-08-02 11:40:00
Location Latitude 41.93695 Google Maps OpenStreetMap
Location Longitude -87.89361 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 10
Recovered Bbls 3.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2014-08-02 11:40:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Product Transferred To Another Tank. Pipeline Was Not Active At The Time
On Site Datetime 2014-08-02 11:40:00
Nrc Rpt Datetime 2014-08-02 15:09:00
Nrc Rpt Num 1091089 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Chicago Terminal #206
Segment Name Tank #715
Onshore State Abbreviation Il
Onshore Postal Code 60131
Onshore City Name Franklin Park
Onshore County Name Cook
Designated Location Milepost/valve Station
Designated Name 304.58
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Api Std Out Of Service Year 1998
Api Std In Service Year 2010
Installation Year 1951
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 25000
Est Cost Emergency 10000
Est Cost Environmental 60000
Est Cost Other 0
Prpty 96000
Accident Psig 9
Mop Psig 13
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was caused by corrosion in the tank floor. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Localized Coating Failure
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Area Of Coating Failure
Corrosion Inhibitors No
Corrosion Lining Yes
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7337
Prepared Date 2015-09-18 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated.

All rights reserved. Copyright © by ClearPHMSA