Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-08-02 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$25,000
Incident datetime
2014-08-02 11:40
Report number
Location
OK
Narrative
Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated.
Detailed record list
Report Received Date
2014-09-02 00:00:00
Iyear
2014
Report Number
20140311
Supplemental Number
20753
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-08-02 11:40:00
Location Latitude
41.93695
Location Longitude
-87.89361
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
10
Recovered Bbls
3.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2014-08-02 11:40:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Product Transferred To Another Tank. Pipeline Was Not Active At The Time
On Site Datetime
2014-08-02 11:40:00
Nrc Rpt Datetime
2014-08-02 15:09:00
Nrc Rpt Num
1091089
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Chicago Terminal #206
Segment Name
Tank #715
Onshore State Abbreviation
Il
Onshore Postal Code
60131
Onshore City Name
Franklin Park
Onshore County Name
Cook
Designated Location
Milepost/valve Station
Designated Name
304.58
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Api Std Out Of Service Year
1998
Api Std In Service Year
2010
Installation Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
25000
Est Cost Emergency
10000
Est Cost Environmental
60000
Est Cost Other
0
Prpty
96000
Accident Psig
9
Mop Psig
13
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was caused by corrosion in the tank floor. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Localized Coating Failure
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Area Of Coating Failure
Corrosion Inhibitors
No
Corrosion Lining
Yes
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7337
Prepared Date
2015-09-18 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated.
| Report Received Date | 2014-09-02 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140311 |
| Supplemental Number | 20753 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2014-08-02 11:40:00 |
| Location Latitude | 41.93695 Google Maps OpenStreetMap |
| Location Longitude | -87.89361 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 10 |
| Recovered Bbls | 3.3 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Contractor Working For The Operator |
| Incident Identified Datetime | 2014-08-02 11:40:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Product Transferred To Another Tank. Pipeline Was Not Active At The Time |
| On Site Datetime | 2014-08-02 11:40:00 |
| Nrc Rpt Datetime | 2014-08-02 15:09:00 |
| Nrc Rpt Num | 1091089 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Chicago Terminal #206 |
| Segment Name | Tank #715 |
| Onshore State Abbreviation | Il |
| Onshore Postal Code | 60131 |
| Onshore City Name | Franklin Park |
| Onshore County Name | Cook |
| Designated Location | Milepost/valve Station |
| Designated Name | 304.58 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Single Bottom System |
| Tank Type | Atmospheric |
| Api Std Out Of Service Year | 1998 |
| Api Std In Service Year | 2010 |
| Installation Year | 1951 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 1000 |
| Est Cost Prop Damage | 25000 |
| Est Cost Emergency | 10000 |
| Est Cost Environmental | 60000 |
| Est Cost Other | 0 |
| Prpty | 96000 |
| Accident Psig | 9 |
| Mop Psig | 13 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The release was caused by corrosion in the tank floor. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Other Corrosion Ind | Yes |
| Int Corrosion Type Details | Localized Coating Failure |
| Int Field Exam Basis Ind | Yes |
| Int Other Loc Ind | Yes |
| Corrosion Location Details | Area Of Coating Failure |
| Corrosion Inhibitors | No |
| Corrosion Lining | Yes |
| Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
| Corrosion Coupons | Not Applicable - Not Mainline Pipe |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7337 |
| Prepared Date | 2015-09-18 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | Contractor personnel working in the magellan chicago facility noticed what appeared to be a product stain around the base of breakout tank 715 accompanied by an aroma of product. Contents of the tank were transferred to another tank and a tank inspection crew was engaged to clean out and inspect the tank. A pinhole was found in the tank floor which was repaired according to company procedures. An API 653 out-of-service inspection was performed, after which a new liner was installed and the tank returned to service. Approximately 8 cubic yards of impacted soil was remediated. |
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