Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-07-26 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,200
Incident datetime
2014-07-26 00:10
Report number
Location
OK
Narrative
Seal failed on tank mixer due to normal wear and tear of goods. The seal was replaced the same day and returned to service.
Detailed record list
Report Received Date
2014-08-18 00:00:00
Iyear
2014
Report Number
20140292
Supplemental Number
19817
Report Type
Supplemental Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-07-26 00:10:00
Location Latitude
29.752401
Location Longitude
-95.207068
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Condensate
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-07-26 00:10:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Inactive At The Time Of The Release And Not Necessary To Shut Down Line
On Site Datetime
2014-07-26 00:15:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal # 474
Segment Name
Tank 416
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Type
Atmospheric
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
1200
Est Cost Emergency
300
Est Cost Environmental
0
Est Cost Other
0
Prpty
1500
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
D******* C*********
Preparer Title
Compliance Coordinator Sr
Preparer Email
D******************@m*********.com
Prepared Date
2014-10-23 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
918-574-7386
Authorizer Email
No Email Address
Narrative
Seal failed on tank mixer due to normal wear and tear of goods. The seal was replaced the same day and returned to service.
| Report Received Date | 2014-08-18 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140292 |
| Supplemental Number | 19817 |
| Report Type | Supplemental Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2014-07-26 00:10:00 |
| Location Latitude | 29.752401 Google Maps OpenStreetMap |
| Location Longitude | -95.207068 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Other |
| Commodity Details | Condensate |
| Unintentional Release Bbls | 0.71 |
| Recovered Bbls | 0.71 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-07-26 00:10:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Tank Was Inactive At The Time Of The Release And Not Necessary To Shut Down Line |
| On Site Datetime | 2014-07-26 00:15:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park Terminal # 474 |
| Segment Name | Tank 416 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Galena Park |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | 0+00 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Tank/vessel |
| Tank Type | Atmospheric |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 1200 |
| Est Cost Emergency | 300 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 1500 |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | D******* C********* |
| Preparer Title | Compliance Coordinator Sr |
| Preparer Email | D******************@m*********.com |
| Prepared Date | 2014-10-23 00:00:00 |
| Authorizer Name | D******* C********* |
| Authorizer Telephone | 918-574-7386 |
| Authorizer Email | No Email Address |
| Narrative | Seal failed on tank mixer due to normal wear and tear of goods. The seal was replaced the same day and returned to service. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA