Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-07-26 — TX
Operator
White Cliffs Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100
Incident datetime
2014-07-26 05:09
Report number
Location
TX
Narrative
A 2' drain line was inadvertently left partially opened while commissioning the wc ii pipeline. When oil was introduced into the scraper trap the sump filled up and overflowed.
Detailed record list
Report Received Date
2014-08-13 00:00:00
Iyear
2014
Report Number
20140290
Supplemental Number
19655
Report Type
Original
Operator Id
32288
Name
White Cliffs Pipeline, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-07-26 05:09:00
Location Latitude
39.04758
Location Longitude
-101.73915
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-07-26 05:09:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2014-07-26 05:09:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Sharon Springs Station
Onshore State Abbreviation
Ks
Onshore Postal Code
67758
Onshore County Name
Wallace
Designated Location
Milepost/valve Station
Designated Name
173.8
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Release Type
Leak
Leak Type
Other
Leak Type Other
Valve Not Fully Closed
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
100
Est Cost Emergency
2000
Est Cost Environmental
4000
Est Cost Other
0
Prpty
6500
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Preparer Name
R**** S******
Preparer Title
District Manager
Preparer Email
R*******@s***********.com
Preparer Telephone
620-234-5532
Prepared Date
2014-08-13 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
918-524-8109
Authorizer Title
Dot Compliance Specialist Sr
Authorizer Email
T********@s***********.com
Narrative
A 2' drain line was inadvertently left partially opened while commissioning the wc ii pipeline. When oil was introduced into the scraper trap the sump filled up and overflowed.
| Report Received Date | 2014-08-13 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140290 |
| Supplemental Number | 19655 |
| Report Type | Original |
| Operator Id | 32288 PHMSA Enforcement |
| Name | White Cliffs Pipeline, Llc |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2014-07-26 05:09:00 |
| Location Latitude | 39.04758 Google Maps OpenStreetMap |
| Location Longitude | -101.73915 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 4 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-07-26 05:09:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| On Site Datetime | 2014-07-26 05:09:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Sharon Springs Station |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67758 |
| Onshore County Name | Wallace |
| Designated Location | Milepost/valve Station |
| Designated Name | 173.8 |
| Federal | No |
| Location Type | Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Auxiliary Piping (E.g. Drain Lines) |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Valve Not Fully Closed |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 400 |
| Est Cost Prop Damage | 100 |
| Est Cost Emergency | 2000 |
| Est Cost Environmental | 4000 |
| Est Cost Other | 0 |
| Prpty | 6500 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
| Operation Type | Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow |
| Preparer Name | R**** S****** |
| Preparer Title | District Manager |
| Preparer Email | R*******@s***********.com |
| Preparer Telephone | 620-234-5532 |
| Prepared Date | 2014-08-13 00:00:00 |
| Authorizer Name | T*** A******* |
| Authorizer Telephone | 918-524-8109 |
| Authorizer Title | Dot Compliance Specialist Sr |
| Authorizer Email | T********@s***********.com |
| Narrative | A 2' drain line was inadvertently left partially opened while commissioning the wc ii pipeline. When oil was introduced into the scraper trap the sump filled up and overflowed. |
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