Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-07-22 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2014-07-22 13:30
Report number
Location
OK
Narrative
Valve 47, which is a motor operated valve located on the #551 tank line inside of sunset station, was found to be inadvertently closed as a result of an electrical malfunction in the valve actuator from moisture build up from an unknown cause. The closing of valve 47 blocked in a segment of 551 tank line without thermal protection. The east operator on duty found a flange to be leaking on the unprotected segment of the 551 tank line inside of the el dorado east station. Pans were immediately placed under the leak and a vacuum truck truck was called to assist with the recovery of product. This line segment was drained down and the affected flange was broken down and a new gasket was installed. Valve 47 and several other valves have been manually opened pending the completion of a project to remove several valves and replace them with a spoool of pre-tested pipe.
Detailed record list
Report Received Date
2014-08-11 00:00:00
Iyear
2014
Report Number
20140286
Supplemental Number
19972
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-07-22 13:30:00
Location Latitude
37.80225
Location Longitude
-96.87537
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.2
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-07-22 13:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Was Down At The Time, And Did Not Shut Down Due To The Incident
On Site Datetime
2014-07-22 13:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
El Dorado East Station
Segment Name
Station #556
Onshore State Abbreviation
Ks
Onshore Postal Code
67042
Onshore City Name
El Dorado
Onshore County Name
Butler
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Gasket On Tank Line
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket Leaked
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
1000
Est Cost Other
0
Prpty
1535
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2014-12-12 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Valve 47, which is a motor operated valve located on the #551 tank line inside of sunset station, was found to be inadvertently closed as a result of an electrical malfunction in the valve actuator from moisture build up from an unknown cause. The closing of valve 47 blocked in a segment of 551 tank line without thermal protection. The east operator on duty found a flange to be leaking on the unprotected segment of the 551 tank line inside of the el dorado east station. Pans were immediately placed under the leak and a vacuum truck truck was called to assist with the recovery of product. This line segment was drained down and the affected flange was broken down and a new gasket was installed. Valve 47 and several other valves have been manually opened pending the completion of a project to remove several valves and replace them with a spoool of pre-tested pipe.
| Report Received Date | 2014-08-11 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140286 |
| Supplemental Number | 19972 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2014-07-22 13:30:00 |
| Location Latitude | 37.80225 Google Maps OpenStreetMap |
| Location Longitude | -96.87537 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
| Unintentional Release Bbls | 0.2 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-07-22 13:30:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The Line Was Down At The Time, And Did Not Shut Down Due To The Incident |
| On Site Datetime | 2014-07-22 13:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | El Dorado East Station |
| Segment Name | Station #556 |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67042 |
| Onshore City Name | El Dorado |
| Onshore County Name | Butler |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Gasket On Tank Line |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Gasket Leaked |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 35 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 500 |
| Est Cost Environmental | 1000 |
| Est Cost Other | 0 |
| Prpty | 1535 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Malfunction Of Control/relief Equipment |
| Eq Failure Type | Malfunction Of Control/relief Equipment |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7377 |
| Prepared Date | 2014-12-12 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | Valve 47, which is a motor operated valve located on the #551 tank line inside of sunset station, was found to be inadvertently closed as a result of an electrical malfunction in the valve actuator from moisture build up from an unknown cause. The closing of valve 47 blocked in a segment of 551 tank line without thermal protection. The east operator on duty found a flange to be leaking on the unprotected segment of the 551 tank line inside of the el dorado east station. Pans were immediately placed under the leak and a vacuum truck truck was called to assist with the recovery of product. This line segment was drained down and the affected flange was broken down and a new gasket was installed. Valve 47 and several other valves have been manually opened pending the completion of a project to remove several valves and replace them with a spoool of pre-tested pipe. |
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