HL incident on 2014-07-10 — TX

Operator
Rose Rock Midstream L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2014-07-10 07:00
Report number
Location
TX
Narrative
A check valve on the discharge of the no. 1 pump unit failed to seal allowing discharge pressure to enter the low pressure piping on the suction side of the pump unit. The pressure relief valve operated according to design and relieved the pressure to the sump. Included in the sump drain line system was a containment pan which overflowed approximately 15 gallons into the gravel surrounding the pan.
Detailed record list
Report Received Date
2014-08-06 00:00:00
Iyear
2014
Report Number
20140281
Supplemental Number
19937
Report Type
Supplemental Final
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-07-10 07:00:00
Location Latitude
Location Longitude
-97.29606047
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-07-10 07:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
On Site Datetime
2014-07-10 08:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
See Station
Segment Name
See To Cushing Trunkline
Onshore State Abbreviation
Ok
Onshore Postal Code
74630
Onshore City Name
Billings
Onshore County Name
Garfield
Designated Location
Milepost/valve Station
Designated Name
Mp 1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Sump
Release Type
Overfill Or Overflow
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1550
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
E*** N********
Preparer Title
District Manager
Preparer Email
E*********@s***********.com
Preparer Telephone
918-225-7758
Preparer Fax
918-225-2579
Prepared Date
2014-12-05 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
918-524-8109
Authorizer Title
Dot Compliance Specialist Sr
Authorizer Email
T********@s***********.com
Narrative
A check valve on the discharge of the no. 1 pump unit failed to seal allowing discharge pressure to enter the low pressure piping on the suction side of the pump unit. The pressure relief valve operated according to design and relieved the pressure to the sump. Included in the sump drain line system was a containment pan which overflowed approximately 15 gallons into the gravel surrounding the pan.
Report Received Date 2014-08-06 00:00:00
Iyear 2014
Report Number 20140281
Supplemental Number 19937
Report Type Supplemental Final
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-07-10 07:00:00
Location Latitude 36.55711482 Google Maps OpenStreetMap
Location Longitude -97.29606047 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-07-10 07:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
On Site Datetime 2014-07-10 08:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name See Station
Segment Name See To Cushing Trunkline
Onshore State Abbreviation Ok
Onshore Postal Code 74630
Onshore City Name Billings
Onshore County Name Garfield
Designated Location Milepost/valve Station
Designated Name Mp 1
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Sump
Release Type Overfill Or Overflow
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1550
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Preparer Name E*** N********
Preparer Title District Manager
Preparer Email E*********@s***********.com
Preparer Telephone 918-225-7758
Preparer Fax 918-225-2579
Prepared Date 2014-12-05 00:00:00
Authorizer Name T*** A*******
Authorizer Telephone 918-524-8109
Authorizer Title Dot Compliance Specialist Sr
Authorizer Email T********@s***********.com
Narrative A check valve on the discharge of the no. 1 pump unit failed to seal allowing discharge pressure to enter the low pressure piping on the suction side of the pump unit. The pressure relief valve operated according to design and relieved the pressure to the sump. Included in the sump drain line system was a containment pan which overflowed approximately 15 gallons into the gravel surrounding the pan.

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