HL incident on 2014-07-04 — TX

Operator
Tesoro Socal Pipeline Company Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50,000
Incident datetime
2014-07-04 00:30
Report number
Location
TX
Narrative
On july 4, 2014, at approximately 0035, operator personnel discovered oil in a retention pond at the carson crude terminal. The control center was immediately notified and all pipelines in the vicinity were shutdown. Several pipeline operators, who have lines which run through the carson crude terminal, were notified and came on site. Once the piping was isolated and soil removed, tesoro discovered its line 63x leaking at approximately 13:00 hours and subsequently clamped it. The failed segment of line was subsequently removed and sent to a metallurgical laboratory for failure analysis. All free standing oil has been recovered and soil remediation is ongoing. There was no impact outside of the tesoro property. A metallurgical analysis(october 2014) revealed that the failure was most likely caused by a combination of microbes and oxygen and the line segment being static .
Detailed record list
Report Received Date
2014-08-05 00:00:00
Iyear
2014
Report Number
20140280
Supplemental Number
20320
Report Type
Supplemental Final
Operator Id
Name
Tesoro Socal Pipeline Company Llc
Operator Street Address
19100 Ridgewood Parkway
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78259
Local Datetime
2014-07-04 00:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
225
Recovered Bbls
225
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2014-07-04 00:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-07-04 00:35:00
Restart Datetime
2014-07-11 13:53:00
On Site Datetime
2014-07-04 01:00:00
Nrc Rpt Datetime
2014-07-04 02:56:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Carson Crude Terminal
Segment Name
Line 63x
Onshore State Abbreviation
Ca
Onshore Postal Code
90745
Onshore City Name
Carson
Onshore County Name
Los Angeles
Designated Location
Survey Station No.
Designated Name
19+59
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
40
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.219
Pipe Smys
52000
Pipe Specification
X52
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1978
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
Yes
Birds Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1200
Est Cost Prop Damage
50000
Est Cost Emergency
25000
Est Cost Environmental
200000
Est Cost Other
5000
Est Cost Other Details
Security To Control Terminal Entry.
Prpty
281200
Accident Psig
2
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
General Corrosion
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
This Section Of Piping Was Just Downstream Of A Tee Joint Separating Flow Path. The Path Seeing The Corrosion Was Part Of A Static Active(Dead Leg) Portion Of The Pipeline.
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2013
Hydrtst Most Rcnt Pressure
1097
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J**** R* M****
Preparer Title
Senior Regulatory Compliance Specialist
Preparer Email
J************@t******.com
Preparer Telephone
210-626-6067
Prepared Date
2015-04-09 00:00:00
Authorizer Name
A**** M*******
Authorizer Telephone
2106266343
Authorizer Email
A***************@t******.com
Narrative
On july 4, 2014, at approximately 0035, operator personnel discovered oil in a retention pond at the carson crude terminal. The control center was immediately notified and all pipelines in the vicinity were shutdown. Several pipeline operators, who have lines which run through the carson crude terminal, were notified and came on site. Once the piping was isolated and soil removed, tesoro discovered its line 63x leaking at approximately 13:00 hours and subsequently clamped it. The failed segment of line was subsequently removed and sent to a metallurgical laboratory for failure analysis. All free standing oil has been recovered and soil remediation is ongoing. There was no impact outside of the tesoro property. A metallurgical analysis(october 2014) revealed that the failure was most likely caused by a combination of microbes and oxygen and the line segment being static .
Report Received Date 2014-08-05 00:00:00
Iyear 2014
Report Number 20140280
Supplemental Number 20320
Report Type Supplemental Final
Operator Id 39013 PHMSA Enforcement
Name Tesoro Socal Pipeline Company Llc
Operator Street Address 19100 Ridgewood Parkway
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78259
Local Datetime 2014-07-04 00:30:00
Location Latitude 33.803335 Google Maps OpenStreetMap
Location Longitude -118.254678 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 225
Recovered Bbls 225
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2014-07-04 00:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-07-04 00:35:00
Restart Datetime 2014-07-11 13:53:00
On Site Datetime 2014-07-04 01:00:00
Nrc Rpt Datetime 2014-07-04 02:56:00
Nrc Rpt Num 1088021 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Carson Crude Terminal
Segment Name Line 63x
Onshore State Abbreviation Ca
Onshore Postal Code 90745
Onshore City Name Carson
Onshore County Name Los Angeles
Designated Location Survey Station No.
Designated Name 19+59
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 40
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.219
Pipe Smys 52000
Pipe Specification X52
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1978
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind Yes
Birds Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1200
Est Cost Prop Damage 50000
Est Cost Emergency 25000
Est Cost Environmental 200000
Est Cost Other 5000
Est Cost Other Details Security To Control Terminal Entry.
Prpty 281200
Accident Psig 2
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results General Corrosion
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details This Section Of Piping Was Just Downstream Of A Tee Joint Separating Flow Path. The Path Seeing The Corrosion Was Part Of A Static Active(Dead Leg) Portion Of The Pipeline.
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2013
Hydrtst Most Rcnt Pressure 1097
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J**** R* M****
Preparer Title Senior Regulatory Compliance Specialist
Preparer Email J************@t******.com
Preparer Telephone 210-626-6067
Prepared Date 2015-04-09 00:00:00
Authorizer Name A**** M*******
Authorizer Telephone 2106266343
Authorizer Email A***************@t******.com
Narrative On july 4, 2014, at approximately 0035, operator personnel discovered oil in a retention pond at the carson crude terminal. The control center was immediately notified and all pipelines in the vicinity were shutdown. Several pipeline operators, who have lines which run through the carson crude terminal, were notified and came on site. Once the piping was isolated and soil removed, tesoro discovered its line 63x leaking at approximately 13:00 hours and subsequently clamped it. The failed segment of line was subsequently removed and sent to a metallurgical laboratory for failure analysis. All free standing oil has been recovered and soil remediation is ongoing. There was no impact outside of the tesoro property. A metallurgical analysis(october 2014) revealed that the failure was most likely caused by a combination of microbes and oxygen and the line segment being static .

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