HL incident on 2014-05-24 — TX

Operator
Holly Energy Partners - Operating, L.p.
Cause
Miscellaneous Root Causes
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$400,000
Incident datetime
2014-05-24 12:00
Report number
Location
TX
Narrative
On saturday, may 24, 2014, equipment operated by willbros t&d services struck hep fintex/trust river, l.P.'s fintex pipeline while digging a hole to a depth of approximately 20 ft. On the easement of the fintex pipeline. As a result of willbros rupture on the fintex pipeline, gasoline was released from the pipeline and a significant quantity of the released gasoline traveled to and along a nearby highway before it ignited. On 7/24/2014, sections a 9 was updated and section d 8(b) total dollars of commodity lost.
Detailed record list
Report Received Date
2014-06-24 00:00:00
Iyear
2014
Report Number
20140247
Supplemental Number
19594
Report Type
Supplemental Final
Operator Id
Name
Holly Energy Partners - Operating, L.p.
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2014-05-24 11:44:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
890
Recovered Bbls
103
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-05-24 12:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Not Transporting Product At The Time Of The Incident.
On Site Datetime
2014-05-24 14:30:00
Nrc Rpt Datetime
2014-05-24 13:20:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Pipe Fac Name
10" Fintex
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
268
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.365
Pipe Smys
42000
Pipe Specification
5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Us Steel
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2009
Manufactured Year
2009
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
2
Puncture Circum
2
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
103
Rel Water Name
The Name Of The Body Of Water Is Unknown At This Time. Please Note That The Answer In 5.b Is The Total Volume Of Gasoline That Has Been Recovered From The Water. The Total Water/gasoline Mixture That Has Been Recovered And Disposed Of At This Time Is 1416 Bbls.
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
950000
Est Cost Gas Released
111250
Est Cost Prop Damage
400000
Est Cost Emergency
80000
Est Cost Environmental
1500000
Est Cost Other
0
Prpty
3041250
Accident Psig
323
Mop Psig
753
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
31680
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident occurred due to third-party damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Contractor
Excavator Equipment
Auger
Work Performed
Pole
One Call Notified Ind
No
Locator Type
Utility Owner
Visible Marks
Yes
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
The Excavator Was Excavating With An Expired One-Call Ticket.
Preparer Name
S****** E*******
Preparer Title
Sr. Regulatory Coordinator
Preparer Email
S***************@h**********.com
Preparer Telephone
575-748-8943
Preparer Fax
214-540-1325
Prepared Date
2014-07-24 00:00:00
Authorizer Name
S****** E*******
Authorizer Telephone
575-748-8943
Authorizer Title
Sr. Regulatory Coordinator
Authorizer Email
S***************@h**********.com
Narrative
On saturday, may 24, 2014, equipment operated by willbros t&d services struck hep fintex/trust river, l.P.'s fintex pipeline while digging a hole to a depth of approximately 20 ft. On the easement of the fintex pipeline. As a result of willbros rupture on the fintex pipeline, gasoline was released from the pipeline and a significant quantity of the released gasoline traveled to and along a nearby highway before it ignited. On 7/24/2014, sections a 9 was updated and section d 8(b) total dollars of commodity lost.
Report Received Date 2014-06-24 00:00:00
Iyear 2014
Report Number 20140247
Supplemental Number 19594
Report Type Supplemental Final
Operator Id 32011 PHMSA Enforcement
Name Holly Energy Partners - Operating, L.p.
Operator Street Address 2323 Victory Ave. Suite 1400
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75219
Local Datetime 2014-05-24 11:44:00
Location Latitude 31.968284 Google Maps OpenStreetMap
Location Longitude -102.07291 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 890
Recovered Bbls 103
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2014-05-24 12:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Not Transporting Product At The Time Of The Incident.
On Site Datetime 2014-05-24 14:30:00
Nrc Rpt Datetime 2014-05-24 13:20:00
Nrc Rpt Num 1083809 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Pipe Fac Name 10" Fintex
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 268
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.365
Pipe Smys 42000
Pipe Specification 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Us Steel
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2009
Manufactured Year 2009
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 2
Puncture Circum 2
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 103
Rel Water Name The Name Of The Body Of Water Is Unknown At This Time. Please Note That The Answer In 5.b Is The Total Volume Of Gasoline That Has Been Recovered From The Water. The Total Water/gasoline Mixture That Has Been Recovered And Disposed Of At This Time Is 1416 Bbls.
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 950000
Est Cost Gas Released 111250
Est Cost Prop Damage 400000
Est Cost Emergency 80000
Est Cost Environmental 1500000
Est Cost Other 0
Prpty 3041250
Accident Psig 323
Mop Psig 753
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 31680
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident occurred due to third-party damage.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype State Highway
Excavator Type Contractor
Excavator Equipment Auger
Work Performed Pole
One Call Notified Ind No
Locator Type Utility Owner
Visible Marks Yes
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other The Excavator Was Excavating With An Expired One-Call Ticket.
Preparer Name S****** E*******
Preparer Title Sr. Regulatory Coordinator
Preparer Email S***************@h**********.com
Preparer Telephone 575-748-8943
Preparer Fax 214-540-1325
Prepared Date 2014-07-24 00:00:00
Authorizer Name S****** E*******
Authorizer Telephone 575-748-8943
Authorizer Title Sr. Regulatory Coordinator
Authorizer Email S***************@h**********.com
Narrative On saturday, may 24, 2014, equipment operated by willbros t&d services struck hep fintex/trust river, l.P.'s fintex pipeline while digging a hole to a depth of approximately 20 ft. On the easement of the fintex pipeline. As a result of willbros rupture on the fintex pipeline, gasoline was released from the pipeline and a significant quantity of the released gasoline traveled to and along a nearby highway before it ignited. On 7/24/2014, sections a 9 was updated and section d 8(b) total dollars of commodity lost.

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