HL incident on 2014-06-05 — OH

Operator
Marathon Pipe Line Llc
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2014-06-05 02:00
Report number
Location
OH
Narrative
Pipe had been cut for project work to weld in a 20" t. Severe thunderstorms rolled into the area and work was stopped for safety reasons. Received over 2" of rain and the runoff filled the excavation and migrated into the pipe, when the water was being vacuumed out of the excavation, it washed residual oil from the pipe into the excavation area. It was immediately vacuumed up as it was released.
Detailed record list
Report Received Date
2014-06-19 00:00:00
Iyear
2014
Report Number
20140239
Supplemental Number
19639
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2014-06-05 02:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
7.1
Recovered Bbls
7.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-06-05 02:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2014-06-05 02:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Owensboro Station
Segment Name
Patoka-Owensboro 20"
Onshore State Abbreviation
Ky
Onshore Postal Code
42303
Onshore City Name
Owensboro
Onshore County Name
Daviess
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
2011
Material Involved
Carbon Steel
Release Type
Other
Leak Type Other
Weather Related
Release Type Details
Pipe Had Been Cut For The Project Work To Weld In A 20" T. Severe Thunderstorms Rolled Into The Area And Work Was Stopped For Safety Reasons. Received Over 2" Of Rain And The Runoff Filled The Excavation And Migrated Into The Pipe, When The Water Was Vacuumed Out Of The Excavation, It Washed Residual Oil From The Pipe Into The Excavation.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
710
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2210
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Heavy Rains And Flooding In The Area.
Nf Extreme Weather Ind
No
Preparer Name
R**** H********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2014-08-06 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
R*******@m****************.com
Narrative
Pipe had been cut for project work to weld in a 20" t. Severe thunderstorms rolled into the area and work was stopped for safety reasons. Received over 2" of rain and the runoff filled the excavation and migrated into the pipe, when the water was being vacuumed out of the excavation, it washed residual oil from the pipe into the excavation area. It was immediately vacuumed up as it was released.
Report Received Date 2014-06-19 00:00:00
Iyear 2014
Report Number 20140239
Supplemental Number 19639
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2014-06-05 02:00:00
Location Latitude 37.7766173 Google Maps OpenStreetMap
Location Longitude -87.073657 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 7.1
Recovered Bbls 7.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-06-05 02:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
On Site Datetime 2014-06-05 02:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Owensboro Station
Segment Name Patoka-Owensboro 20"
Onshore State Abbreviation Ky
Onshore Postal Code 42303
Onshore City Name Owensboro
Onshore County Name Daviess
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Crossing No
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Installation Year 2011
Material Involved Carbon Steel
Release Type Other
Leak Type Other Weather Related
Release Type Details Pipe Had Been Cut For The Project Work To Weld In A 20" T. Severe Thunderstorms Rolled Into The Area And Work Was Stopped For Safety Reasons. Received Over 2" Of Rain And The Runoff Filled The Excavation And Migrated Into The Pipe, When The Water Was Vacuumed Out Of The Excavation, It Washed Residual Oil From The Pipe Into The Excavation.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 710
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2210
Accident Psig 0
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Other
Nf Other Details Heavy Rains And Flooding In The Area.
Nf Extreme Weather Ind No
Preparer Name R**** H********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2014-08-06 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory Compliance Manager
Authorizer Email R*******@m****************.com
Narrative Pipe had been cut for project work to weld in a 20" t. Severe thunderstorms rolled into the area and work was stopped for safety reasons. Received over 2" of rain and the runoff filled the excavation and migrated into the pipe, when the water was being vacuumed out of the excavation, it washed residual oil from the pipe into the excavation area. It was immediately vacuumed up as it was released.

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