Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-05-20 — TX
Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2014-05-20 09:30
Report number
Location
TX
Narrative
A crude oil release was discovered by operations personnel on 5/20/2014 at evant station on the amdel garden city to nederland 10" pipeline system. The pipeline system was shut down and the station piping was isolated. Investigation revealed the release was from an isolated section of dead leg piping. The dead leg station piping was removed and blinds were installed. Further investigation of evant station revealed that there were no additional dead leg piping sections to be removed.
Detailed record list
Report Received Date
2014-06-18 00:00:00
Iyear
2014
Report Number
20140237
Supplemental Number
19774
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-05-20 09:30:00
Location Latitude
31.4396
Location Longitude
-98.14535
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-05-20 09:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-05-20 09:30:00
Restart Datetime
2014-05-20 17:45:00
On Site Datetime
2014-05-20 09:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Evant Station
Segment Name
21001-10" Nederland To Garden City
Onshore State Abbreviation
Tx
Onshore Postal Code
76525
Onshore City Name
Evant
Onshore County Name
Coryell
Designated Location
Milepost/valve Station
Designated Name
191.95
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
198
Est Cost Prop Damage
0
Est Cost Emergency
20000
Est Cost Environmental
27000
Est Cost Other
0
Prpty
47198
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2014-10-06 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
A crude oil release was discovered by operations personnel on 5/20/2014 at evant station on the amdel garden city to nederland 10" pipeline system. The pipeline system was shut down and the station piping was isolated. Investigation revealed the release was from an isolated section of dead leg piping. The dead leg station piping was removed and blinds were installed. Further investigation of evant station revealed that there were no additional dead leg piping sections to be removed.
| Report Received Date | 2014-06-18 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140237 |
| Supplemental Number | 19774 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2014-05-20 09:30:00 |
| Location Latitude | 31.4396 Google Maps OpenStreetMap |
| Location Longitude | -98.14535 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 2 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-05-20 09:30:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2014-05-20 09:30:00 |
| Restart Datetime | 2014-05-20 17:45:00 |
| On Site Datetime | 2014-05-20 09:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Evant Station |
| Segment Name | 21001-10" Nederland To Garden City |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 76525 |
| Onshore City Name | Evant |
| Onshore County Name | Coryell |
| Designated Location | Milepost/valve Station |
| Designated Name | 191.95 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Release Type | Leak |
| Leak Type | Pinhole |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 198 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 20000 |
| Est Cost Environmental | 27000 |
| Est Cost Other | 0 |
| Prpty | 47198 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Preparer Name | T*** G* N******* |
| Preparer Title | Dot Compliance Manager |
| Preparer Email | T*********@s**************.com |
| Preparer Telephone | 281-637-6576 |
| Preparer Fax | 877-917-0448 |
| Prepared Date | 2014-10-06 00:00:00 |
| Authorizer Name | T*** G* N******* |
| Authorizer Telephone | 281-637-6576 |
| Authorizer Title | Dot Compliance Manager |
| Authorizer Email | T*********@s**************.com |
| Narrative | A crude oil release was discovered by operations personnel on 5/20/2014 at evant station on the amdel garden city to nederland 10" pipeline system. The pipeline system was shut down and the station piping was isolated. Investigation revealed the release was from an isolated section of dead leg piping. The dead leg station piping was removed and blinds were installed. Further investigation of evant station revealed that there were no additional dead leg piping sections to be removed. |
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