HL incident on 2014-05-18 — TX

Operator
Genesis Pipeline Usa, L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-05-18 13:30
Report number
Location
TX
Narrative
On 5/16/2014, a 16" back pressure valve was installed on the facility piping between the pig receiver and the act skid at exxon anchorage tank farm in port allen, la. The new valve was received with 4 red thread protection caps on the face of the valve. Three of the caps were for lifting eyes and the fourth being a direct port to the valves internal components. All four caps were left in place following the intallation. When the station was placed back into service (5/17/2014), the thread protection port to the valves internal components blew out resulting in the release of approxiamtely 20bbls of crude oil which was discovered 5/18/2014. Changes to this accident report on 11/3/2014 were done to fix errors that were found as a result of a ladnr investigation. Supplemental: 9/2/2016 correction to part d question 6 and 7. According to mapping data, the accident occurred within a high population area hca as defined under 195.450.
Detailed record list
Report Received Date
2014-06-13 00:00:00
Iyear
2014
Report Number
20140233
Supplemental Number
21658
Report Type
Supplemental Final
Operator Id
Name
Genesis Pipeline Usa, L.p.
Operator Street Address
811 Louisiana St. Suite 1200
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-05-18 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2014-05-18 13:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-05-18 13:32:00
Restart Datetime
2014-05-20 02:14:00
On Site Datetime
2014-05-18 16:00:00
Nrc Rpt Datetime
2014-05-18 16:06:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tiger Pipeline
Segment Name
Anchorage
Onshore State Abbreviation
La
Onshore Postal Code
70767
Onshore City Name
Port Allen
Onshore County Name
West Baton Rouge
Designated Location
Milepost/valve Station
Designated Name
Anchorage
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Steel Plug Was Not Used
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
0
Est Cost Emergency
94704
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
None
Prpty
95704
Accident Psig
13
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The accident was caused by improper installation of a control valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Inadequate Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
J**** M*****
Preparer Title
Pipeline Compliance Specialist
Preparer Email
J***********@g****.com
Preparer Telephone
225-216-5905
Prepared Date
2016-09-02 00:00:00
Authorizer Name
J*** J*****
Authorizer Telephone
713-860-2500
Authorizer Title
Dot Compliance Manager
Authorizer Email
J**********@g****.com
Narrative
On 5/16/2014, a 16" back pressure valve was installed on the facility piping between the pig receiver and the act skid at exxon anchorage tank farm in port allen, la. The new valve was received with 4 red thread protection caps on the face of the valve. Three of the caps were for lifting eyes and the fourth being a direct port to the valves internal components. All four caps were left in place following the intallation. When the station was placed back into service (5/17/2014), the thread protection port to the valves internal components blew out resulting in the release of approxiamtely 20bbls of crude oil which was discovered 5/18/2014. Changes to this accident report on 11/3/2014 were done to fix errors that were found as a result of a ladnr investigation. Supplemental: 9/2/2016 correction to part d question 6 and 7. According to mapping data, the accident occurred within a high population area hca as defined under 195.450.
Report Received Date 2014-06-13 00:00:00
Iyear 2014
Report Number 20140233
Supplemental Number 21658
Report Type Supplemental Final
Operator Id 31045 PHMSA Enforcement
Name Genesis Pipeline Usa, L.p.
Operator Street Address 811 Louisiana St. Suite 1200
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-05-18 13:30:00
Location Latitude 30.47832 Google Maps OpenStreetMap
Location Longitude -91.21973 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2014-05-18 13:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-05-18 13:32:00
Restart Datetime 2014-05-20 02:14:00
On Site Datetime 2014-05-18 16:00:00
Nrc Rpt Datetime 2014-05-18 16:06:00
Nrc Rpt Num 1083162 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Tiger Pipeline
Segment Name Anchorage
Onshore State Abbreviation La
Onshore Postal Code 70767
Onshore City Name Port Allen
Onshore County Name West Baton Rouge
Designated Location Milepost/valve Station
Designated Name Anchorage
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Steel Plug Was Not Used
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 0
Est Cost Emergency 94704
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details None
Prpty 95704
Accident Psig 13
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The accident was caused by improper installation of a control valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Inadequate Proc Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name J**** M*****
Preparer Title Pipeline Compliance Specialist
Preparer Email J***********@g****.com
Preparer Telephone 225-216-5905
Prepared Date 2016-09-02 00:00:00
Authorizer Name J*** J*****
Authorizer Telephone 713-860-2500
Authorizer Title Dot Compliance Manager
Authorizer Email J**********@g****.com
Narrative On 5/16/2014, a 16" back pressure valve was installed on the facility piping between the pig receiver and the act skid at exxon anchorage tank farm in port allen, la. The new valve was received with 4 red thread protection caps on the face of the valve. Three of the caps were for lifting eyes and the fourth being a direct port to the valves internal components. All four caps were left in place following the intallation. When the station was placed back into service (5/17/2014), the thread protection port to the valves internal components blew out resulting in the release of approxiamtely 20bbls of crude oil which was discovered 5/18/2014. Changes to this accident report on 11/3/2014 were done to fix errors that were found as a result of a ladnr investigation. Supplemental: 9/2/2016 correction to part d question 6 and 7. According to mapping data, the accident occurred within a high population area hca as defined under 195.450.

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