HL incident on 2014-05-12 — TX

Operator
Plantation Pipe Line Co
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-05-12 13:18
Report number
Location
TX
Narrative
On 5/12/2014, a scraper passage indicator (pig sig) was being removed and a new one installed at the incoming block valve on the 26-inch pipeline at plantation's anderson pumping station. Shortly after installation of the new indicator, it failed (blew out) causing a release of gasoline. The investigation of the accident determined an employee was installing the stainless steel pig sig into a previously damaged thread-o-ring (tor) fitting. The installation of the pig sig was being done using a td williamson tapping machine. The stainless steel pig sig did not seat properly in the damaged tor. The employee did not follow the procedure for installing a pig sig.
Detailed record list
Report Received Date
2014-06-10 00:00:00
Iyear
2014
Report Number
20140226
Supplemental Number
19578
Report Type
Supplemental Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana Street Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-05-12 13:18:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
608
Recovered Bbls
163
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-05-12 13:18:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-05-12 13:18:00
Restart Datetime
2014-05-13 18:28:00
On Site Datetime
2014-05-12 13:18:00
Nrc Rpt Datetime
2014-05-12 14:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Cng Pipeline/anderson Pumping Station
Onshore State Abbreviation
Sc
Onshore Postal Code
29621
Onshore City Name
Anderson
Onshore County Name
Anderson
Designated Location
Milepost/valve Station
Designated Name
Cng-26-2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Scraper Passage Indicator (Pig Sig)
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0
Rel Water Name
Unknown
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
70300
Est Cost Prop Damage
0
Est Cost Emergency
900000
Est Cost Environmental
200000
Est Cost Other
0
Prpty
1170300
Accident Psig
313
Mop Psig
809
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
274560
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
Q****** H* F******
Preparer Title
Manager-Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-751-4240
Preparer Fax
770-751-4130
Prepared Date
2014-07-17 00:00:00
Authorizer Name
Q****** H* F******
Authorizer Telephone
770-751-4240
Authorizer Title
Manager-Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
On 5/12/2014, a scraper passage indicator (pig sig) was being removed and a new one installed at the incoming block valve on the 26-inch pipeline at plantation's anderson pumping station. Shortly after installation of the new indicator, it failed (blew out) causing a release of gasoline. The investigation of the accident determined an employee was installing the stainless steel pig sig into a previously damaged thread-o-ring (tor) fitting. The installation of the pig sig was being done using a td williamson tapping machine. The stainless steel pig sig did not seat properly in the damaged tor. The employee did not follow the procedure for installing a pig sig.
Report Received Date 2014-06-10 00:00:00
Iyear 2014
Report Number 20140226
Supplemental Number 19578
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana Street Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-05-12 13:18:00
Location Latitude 34.481971 Google Maps OpenStreetMap
Location Longitude -82.60639 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 608
Recovered Bbls 163
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-05-12 13:18:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-05-12 13:18:00
Restart Datetime 2014-05-13 18:28:00
On Site Datetime 2014-05-12 13:18:00
Nrc Rpt Datetime 2014-05-12 14:27:00
Nrc Rpt Num 1082532 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Cng Pipeline/anderson Pumping Station
Onshore State Abbreviation Sc
Onshore Postal Code 29621
Onshore City Name Anderson
Onshore County Name Anderson
Designated Location Milepost/valve Station
Designated Name Cng-26-2
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Scraper Passage Indicator (Pig Sig)
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0
Rel Water Name Unknown
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 70300
Est Cost Prop Damage 0
Est Cost Emergency 900000
Est Cost Environmental 200000
Est Cost Other 0
Prpty 1170300
Accident Psig 313
Mop Psig 809
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 274560
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name Q****** H* F******
Preparer Title Manager-Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-751-4240
Preparer Fax 770-751-4130
Prepared Date 2014-07-17 00:00:00
Authorizer Name Q****** H* F******
Authorizer Telephone 770-751-4240
Authorizer Title Manager-Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative On 5/12/2014, a scraper passage indicator (pig sig) was being removed and a new one installed at the incoming block valve on the 26-inch pipeline at plantation's anderson pumping station. Shortly after installation of the new indicator, it failed (blew out) causing a release of gasoline. The investigation of the accident determined an employee was installing the stainless steel pig sig into a previously damaged thread-o-ring (tor) fitting. The installation of the pig sig was being done using a td williamson tapping machine. The stainless steel pig sig did not seat properly in the damaged tor. The employee did not follow the procedure for installing a pig sig.

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