HL incident on 2014-05-06 — KS

Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,317
Incident datetime
2014-05-06 16:31
Report number
Location
KS
Narrative
The kaw pipe line companies hill city positive displacement injection pump packing gland failed. Failure was due to the packing gland retainer broke resulting in the loss of packing. Employees onsite from another company witnessed the packing gland failure and disconnected the power to the pumps electric motor and then reported the leak to the controller. The controller secured the remaining parts of the pipeline segment and initiated the emergency response plan. Most clean up was performed on the day of the release. The clean up efforts were conducted with the kansas department of health and enviroment (kdhe) oversight. Some liquid was recovered. The soil is in process of being remediated on site with kdhe's oversight. The hazardous liquid run off remained on site. The investigation reveals that the casual factor was metal fatigue. Approximately 1 yard of soil is being remediated.
Detailed record list
Report Received Date
2014-06-03 00:00:00
Iyear
2014
Report Number
20140219
Supplemental Number
19703
Report Type
Supplemental Final
Operator Id
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 S. Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2014-05-06 16:12:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.9
Recovered Bbls
2.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-05-06 16:31:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-05-06 16:31:00
Restart Datetime
2014-05-08 23:09:00
On Site Datetime
2014-05-06 16:40:00
Nrc Rpt Datetime
2014-05-06 17:16:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Hill City Station
Segment Name
Hill City To Bemis
Onshore State Abbreviation
Ks
Onshore Postal Code
67642
Onshore City Name
Near Hill City
Onshore County Name
Graham
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
1317
Est Cost Emergency
4205
Est Cost Environmental
6633
Est Cost Other
2500
Est Cost Other Details
Investigation Cost
Prpty
14955
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
J**** W*****
Preparer Title
Regulatory Compliance Manager
Preparer Email
J******@n***.coop
Preparer Telephone
6202419253
Prepared Date
2014-09-04 00:00:00
Authorizer Name
J**** W*****
Authorizer Telephone
6202419253
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
J******@n***.coop
Narrative
The kaw pipe line companies hill city positive displacement injection pump packing gland failed. Failure was due to the packing gland retainer broke resulting in the loss of packing. Employees onsite from another company witnessed the packing gland failure and disconnected the power to the pumps electric motor and then reported the leak to the controller. The controller secured the remaining parts of the pipeline segment and initiated the emergency response plan. Most clean up was performed on the day of the release. The clean up efforts were conducted with the kansas department of health and enviroment (kdhe) oversight. Some liquid was recovered. The soil is in process of being remediated on site with kdhe's oversight. The hazardous liquid run off remained on site. The investigation reveals that the casual factor was metal fatigue. Approximately 1 yard of soil is being remediated.
Report Received Date 2014-06-03 00:00:00
Iyear 2014
Report Number 20140219
Supplemental Number 19703
Report Type Supplemental Final
Operator Id 9175 PHMSA Enforcement
Name Jayhawk Pipeline Llc
Operator Street Address 2000 S. Main
Operator City Name Mcpherson
Operator State Abbreviation KS
Operator Postal Code 67460
Local Datetime 2014-05-06 16:12:00
Location Latitude 39.369394 Google Maps OpenStreetMap
Location Longitude -99.80891 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.9
Recovered Bbls 2.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-05-06 16:31:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-05-06 16:31:00
Restart Datetime 2014-05-08 23:09:00
On Site Datetime 2014-05-06 16:40:00
Nrc Rpt Datetime 2014-05-06 17:16:00
Nrc Rpt Num 1081948 NRC Report How to search
Ignite Ind No
Explode Ind No
Pipe Fac Name Hill City Station
Segment Name Hill City To Bemis
Onshore State Abbreviation Ks
Onshore Postal Code 67642
Onshore City Name Near Hill City
Onshore County Name Graham
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Intrastate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 1317
Est Cost Emergency 4205
Est Cost Environmental 6633
Est Cost Other 2500
Est Cost Other Details Investigation Cost
Prpty 14955
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name J**** W*****
Preparer Title Regulatory Compliance Manager
Preparer Email J******@n***.coop
Preparer Telephone 6202419253
Prepared Date 2014-09-04 00:00:00
Authorizer Name J**** W*****
Authorizer Telephone 6202419253
Authorizer Title Regulatory Compliance Manager
Authorizer Email J******@n***.coop
Narrative The kaw pipe line companies hill city positive displacement injection pump packing gland failed. Failure was due to the packing gland retainer broke resulting in the loss of packing. Employees onsite from another company witnessed the packing gland failure and disconnected the power to the pumps electric motor and then reported the leak to the controller. The controller secured the remaining parts of the pipeline segment and initiated the emergency response plan. Most clean up was performed on the day of the release. The clean up efforts were conducted with the kansas department of health and enviroment (kdhe) oversight. Some liquid was recovered. The soil is in process of being remediated on site with kdhe's oversight. The hazardous liquid run off remained on site. The investigation reveals that the casual factor was metal fatigue. Approximately 1 yard of soil is being remediated.

All rights reserved. Copyright © by ClearPHMSA