HL incident on 2014-05-01 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-05-01 13:00
Report number
Location
TX
Narrative
Enterprise pipeline technician was performing maintenance on the mesa meter. After returning the meter back to service, technician observed oil escaping from the mesa meter drain valve causing the sump to overfill. It was discovered that valve was left in the open position. Valve was closed and the leak stopped. Remediation of crude oil was performed. Review of loto procedures was performed for all local employees.
Detailed record list
Report Received Date
2014-05-30 00:00:00
Iyear
2014
Report Number
20140217
Supplemental Number
20010
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-05-01 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-05-01 13:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Accident Did Not Interfere With Facility Operations.
On Site Datetime
2014-05-01 13:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland Tank Farm
Segment Name
Midland Station Mesa Meter
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Other
Leak Type Other
Incorrect Valve Positioning
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
1000
Est Cost Other
0
Prpty
1400
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Preparer Name
S**** D****
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
S******@e****.com
Preparer Telephone
713.381.6487
Prepared Date
2014-12-22 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713.381.6487
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
S******@e****.com
Narrative
Enterprise pipeline technician was performing maintenance on the mesa meter. After returning the meter back to service, technician observed oil escaping from the mesa meter drain valve causing the sump to overfill. It was discovered that valve was left in the open position. Valve was closed and the leak stopped. Remediation of crude oil was performed. Review of loto procedures was performed for all local employees.
Report Received Date 2014-05-30 00:00:00
Iyear 2014
Report Number 20140217
Supplemental Number 20010
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-05-01 13:00:00
Location Latitude 32.019351 Google Maps OpenStreetMap
Location Longitude -102.01641 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-05-01 13:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Accident Did Not Interfere With Facility Operations.
On Site Datetime 2014-05-01 13:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Midland Tank Farm
Segment Name Midland Station Mesa Meter
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Other
Leak Type Other Incorrect Valve Positioning
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 400
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 1000
Est Cost Other 0
Prpty 1400
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Preparer Name S**** D****
Preparer Title Senior Pipeline Compliance Engineer
Preparer Email S******@e****.com
Preparer Telephone 713.381.6487
Prepared Date 2014-12-22 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713.381.6487
Authorizer Title Senior Pipeline Compliance Engineer
Authorizer Email S******@e****.com
Narrative Enterprise pipeline technician was performing maintenance on the mesa meter. After returning the meter back to service, technician observed oil escaping from the mesa meter drain valve causing the sump to overfill. It was discovered that valve was left in the open position. Valve was closed and the leak stopped. Remediation of crude oil was performed. Review of loto procedures was performed for all local employees.

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