HL incident on 2014-04-25 — TX

Operator
Delek Logistics Operating, Llc.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$35,000
Incident datetime
2014-04-25 10:45
Report number
Location
TX
Narrative
At approximately 10:45 am on the morning of april 25, 2014, ariel patrol called glenn green to report a possible leak on the colquitt gathering right-of-way. Glenn green immediately dispatched local field personnel and maitnenance crews to the scene to verify the possible leak and location. Once field personnel and maintenance crews arrived on scene all pumps where shutdown on the system and mainline valves closed. Delek's third party osro was contacted and dispatched to the scene with emergency response equipment, personnel and resources. Supplement: anderson & associates lab analysis was completed and a copy received on june 11, 2014 indicating microbiologically influenced corrosion was the most likely cause. The report has been emailed to southwest region. Pipeline is still out of service pending ili run as of june 30, 2014. Supplement 5 january 2015: received final ili report from tdw on december 16, 2014. Pipeline still out of service. Evaluating financial feasibilty of repairing & restarting line.
Detailed record list
Report Received Date
2014-05-23 00:00:00
Iyear
2014
Report Number
20140202
Supplemental Number
20024
Report Type
Supplemental
Operator Id
Name
Delek Logistics Operating, Llc.
Operator Street Address
5850 Granite Parkway #450
Operator City Name
Plano
Operator State Abbreviation
TX
Operator Postal Code
75024
Local Datetime
2014-04-25 10:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
400
Recovered Bbls
223
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Operator Employee
Incident Identified Datetime
2014-04-25 10:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-25 10:45:00
Still Shutdown Ind
Yes
On Site Datetime
2014-04-25 11:00:00
Nrc Rpt Datetime
2014-04-25 11:41:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Pipe Fac Name
Colquitt Gathering
Segment Name
2202
Onshore State Abbreviation
La
Onshore Postal Code
71038
Onshore City Name
Haynesville
Onshore County Name
Claiborne
Designated Location
Survey Station No.
Designated Name
60+50
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
18
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
35000
Pipe Specification
Api 5l B
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Asphalt
Installation Year
1990
Manufactured Year
1990
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
Yes
Birds Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Wildlife Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
300
Rel Water Name
No Name Dry Drainage Ditch That Discharges Into No Name Creek That Evetually Feeds Doe Branch. No Sign Of Oil Reaching Doe Branch. Doe Branch Is A Tributary Of Cornie Bayou.
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
50000
Est Cost Gas Released
6545
Est Cost Prop Damage
35000
Est Cost Emergency
2500000
Est Cost Environmental
500000
Est Cost Other
250000
Est Cost Other Details
Improve Row Access & Parish Road Repairs
Prpty
3341545
Accident Psig
50
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
24548
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Pit Located At Approximately 4:00 Clock Position In An Underbend For The Drainage Ditch
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2003
Hydrtst Most Rcnt Pressure
900
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
G**** R* G****
Preparer Title
Maintenance Engineering Superintendent
Preparer Email
G**********@l******.com
Preparer Telephone
870-864-1372
Preparer Fax
870-864-1341
Prepared Date
2015-01-05 00:00:00
Authorizer Name
G**** R* G****
Authorizer Telephone
870-864-1372
Authorizer Title
Maintenance Engineering Superintendent
Authorizer Email
G**********@l******.com
Narrative
At approximately 10:45 am on the morning of april 25, 2014, ariel patrol called glenn green to report a possible leak on the colquitt gathering right-of-way. Glenn green immediately dispatched local field personnel and maitnenance crews to the scene to verify the possible leak and location. Once field personnel and maintenance crews arrived on scene all pumps where shutdown on the system and mainline valves closed. Delek's third party osro was contacted and dispatched to the scene with emergency response equipment, personnel and resources. Supplement: anderson & associates lab analysis was completed and a copy received on june 11, 2014 indicating microbiologically influenced corrosion was the most likely cause. The report has been emailed to southwest region. Pipeline is still out of service pending ili run as of june 30, 2014. Supplement 5 january 2015: received final ili report from tdw on december 16, 2014. Pipeline still out of service. Evaluating financial feasibilty of repairing & restarting line.
Report Received Date 2014-05-23 00:00:00
Iyear 2014
Report Number 20140202
Supplemental Number 20024
Report Type Supplemental
Operator Id 11551 PHMSA Enforcement
Name Delek Logistics Operating, Llc.
Operator Street Address 5850 Granite Parkway #450
Operator City Name Plano
Operator State Abbreviation TX
Operator Postal Code 75024
Local Datetime 2014-04-25 10:45:00
Location Latitude 32.97035 Google Maps OpenStreetMap
Location Longitude -92.93675 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 400
Recovered Bbls 223
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Operator Employee
Incident Identified Datetime 2014-04-25 10:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-25 10:45:00
Still Shutdown Ind Yes
On Site Datetime 2014-04-25 11:00:00
Nrc Rpt Datetime 2014-04-25 11:41:00
Nrc Rpt Num 1080818 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Pipe Fac Name Colquitt Gathering
Segment Name 2202
Onshore State Abbreviation La
Onshore Postal Code 71038
Onshore City Name Haynesville
Onshore County Name Claiborne
Designated Location Survey Station No.
Designated Name 60+50
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 18
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys 35000
Pipe Specification Api 5l B
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Asphalt
Installation Year 1990
Manufactured Year 1990
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind Yes
Birds Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Wildlife Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 300
Rel Water Name No Name Dry Drainage Ditch That Discharges Into No Name Creek That Evetually Feeds Doe Branch. No Sign Of Oil Reaching Doe Branch. Doe Branch Is A Tributary Of Cornie Bayou.
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 50000
Est Cost Gas Released 6545
Est Cost Prop Damage 35000
Est Cost Emergency 2500000
Est Cost Environmental 500000
Est Cost Other 250000
Est Cost Other Details Improve Row Access & Parish Road Repairs
Prpty 3341545
Accident Psig 50
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 24548
Internal Inspection Ind Yes
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Pit Located At Approximately 4:00 Clock Position In An Underbend For The Drainage Ditch
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2003
Hydrtst Most Rcnt Pressure 900
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name G**** R* G****
Preparer Title Maintenance Engineering Superintendent
Preparer Email G**********@l******.com
Preparer Telephone 870-864-1372
Preparer Fax 870-864-1341
Prepared Date 2015-01-05 00:00:00
Authorizer Name G**** R* G****
Authorizer Telephone 870-864-1372
Authorizer Title Maintenance Engineering Superintendent
Authorizer Email G**********@l******.com
Narrative At approximately 10:45 am on the morning of april 25, 2014, ariel patrol called glenn green to report a possible leak on the colquitt gathering right-of-way. Glenn green immediately dispatched local field personnel and maitnenance crews to the scene to verify the possible leak and location. Once field personnel and maintenance crews arrived on scene all pumps where shutdown on the system and mainline valves closed. Delek's third party osro was contacted and dispatched to the scene with emergency response equipment, personnel and resources. Supplement: anderson & associates lab analysis was completed and a copy received on june 11, 2014 indicating microbiologically influenced corrosion was the most likely cause. The report has been emailed to southwest region. Pipeline is still out of service pending ili run as of june 30, 2014. Supplement 5 january 2015: received final ili report from tdw on december 16, 2014. Pipeline still out of service. Evaluating financial feasibilty of repairing & restarting line.

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