Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-04-22 — TX
Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,000
Incident datetime
2014-04-22 01:34
Report number
Location
TX
Narrative
Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report
Detailed record list
Report Received Date
2014-05-20 00:00:00
Iyear
2014
Report Number
20140195
Supplemental Number
20537
Report Type
Supplemental Final
Operator Id
31684
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2014-04-22 01:34:00
Location Latitude
30.170532
Location Longitude
-93.339358
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.9
Recovered Bbls
0.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-04-22 01:34:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-22 01:34:00
Restart Datetime
2014-04-22 02:00:00
On Site Datetime
2014-04-22 01:34:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lake Charles Pipeline Facility
Segment Name
Tank 13 Booster Pump
Onshore State Abbreviation
La
Onshore Postal Code
70665
Onshore City Name
Sulphur
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
Tank 13 Boost
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1963
Material Involved
Material Other Than Carbon Steel
Material Details
Seal Material
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
120
Est Cost Prop Damage
1000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2120
Accident Psig
75
Mop Psig
150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was related to a pump seal. Controller was alarmed of seal failure, operations investigated alarm and confirmed seal failure. Controller then isolated pump for repairs.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Breakdown Ind
Yes
Preparer Name
T*** F****
Preparer Title
Dot Coordinator
Preparer Email
M***********@p**.com
Preparer Telephone
832-765-1632
Prepared Date
2015-06-22 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report
| Report Received Date | 2014-05-20 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140195 |
| Supplemental Number | 20537 |
| Report Type | Supplemental Final |
| Operator Id | 31684 PHMSA Enforcement |
| Name | Phillips 66 Pipeline Llc |
| Operator Street Address | 2331 Citywest Blvd |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77042 |
| Local Datetime | 2014-04-22 01:34:00 |
| Location Latitude | 30.170532 Google Maps OpenStreetMap |
| Location Longitude | -93.339358 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 0.9 |
| Recovered Bbls | 0.9 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations) |
| Incident Identified Datetime | 2014-04-22 01:34:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2014-04-22 01:34:00 |
| Restart Datetime | 2014-04-22 02:00:00 |
| On Site Datetime | 2014-04-22 01:34:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Lake Charles Pipeline Facility |
| Segment Name | Tank 13 Booster Pump |
| Onshore State Abbreviation | La |
| Onshore Postal Code | 70665 |
| Onshore City Name | Sulphur |
| Onshore County Name | Calcasieu |
| Designated Location | Milepost/valve Station |
| Designated Name | Tank 13 Boost |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Installation Year | 1963 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Seal Material |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Commercially Nav Ind | Yes |
| Commercially Nav Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 120 |
| Est Cost Prop Damage | 1000 |
| Est Cost Emergency | 1000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2120 |
| Accident Psig | 75 |
| Mop Psig | 150 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Leak was related to a pump seal. Controller was alarmed of seal failure, operations investigated alarm and confirmed seal failure. Controller then isolated pump for repairs. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Other Pump Ind | Seal/packing Failure |
| Additional Breakdown Ind | Yes |
| Preparer Name | T*** F**** |
| Preparer Title | Dot Coordinator |
| Preparer Email | M***********@p**.com |
| Preparer Telephone | 832-765-1632 |
| Prepared Date | 2015-06-22 00:00:00 |
| Authorizer Name | T*** F**** |
| Authorizer Telephone | 832-765-1632 |
| Authorizer Title | Director Dot Compliance |
| Authorizer Email | M***********@p**.com |
| Narrative | Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA