HL incident on 2014-04-22 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2014-04-22 01:34
Report number
Location
TX
Narrative
Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report
Detailed record list
Report Received Date
2014-05-20 00:00:00
Iyear
2014
Report Number
20140195
Supplemental Number
20537
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2014-04-22 01:34:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.9
Recovered Bbls
0.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-04-22 01:34:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-22 01:34:00
Restart Datetime
2014-04-22 02:00:00
On Site Datetime
2014-04-22 01:34:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lake Charles Pipeline Facility
Segment Name
Tank 13 Booster Pump
Onshore State Abbreviation
La
Onshore Postal Code
70665
Onshore City Name
Sulphur
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
Tank 13 Boost
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1963
Material Involved
Material Other Than Carbon Steel
Material Details
Seal Material
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
120
Est Cost Prop Damage
1000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2120
Accident Psig
75
Mop Psig
150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was related to a pump seal. Controller was alarmed of seal failure, operations investigated alarm and confirmed seal failure. Controller then isolated pump for repairs.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Breakdown Ind
Yes
Preparer Name
T*** F****
Preparer Title
Dot Coordinator
Preparer Email
M***********@p**.com
Preparer Telephone
832-765-1632
Prepared Date
2015-06-22 00:00:00
Authorizer Name
T*** F****
Authorizer Telephone
832-765-1632
Authorizer Title
Director Dot Compliance
Authorizer Email
M***********@p**.com
Narrative
Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report
Report Received Date 2014-05-20 00:00:00
Iyear 2014
Report Number 20140195
Supplemental Number 20537
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2014-04-22 01:34:00
Location Latitude 30.170532 Google Maps OpenStreetMap
Location Longitude -93.339358 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.9
Recovered Bbls 0.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2014-04-22 01:34:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-22 01:34:00
Restart Datetime 2014-04-22 02:00:00
On Site Datetime 2014-04-22 01:34:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lake Charles Pipeline Facility
Segment Name Tank 13 Booster Pump
Onshore State Abbreviation La
Onshore Postal Code 70665
Onshore City Name Sulphur
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name Tank 13 Boost
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1963
Material Involved Material Other Than Carbon Steel
Material Details Seal Material
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 120
Est Cost Prop Damage 1000
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 2120
Accident Psig 75
Mop Psig 150
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was related to a pump seal. Controller was alarmed of seal failure, operations investigated alarm and confirmed seal failure. Controller then isolated pump for repairs.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Breakdown Ind Yes
Preparer Name T*** F****
Preparer Title Dot Coordinator
Preparer Email M***********@p**.com
Preparer Telephone 832-765-1632
Prepared Date 2015-06-22 00:00:00
Authorizer Name T*** F****
Authorizer Telephone 832-765-1632
Authorizer Title Director Dot Compliance
Authorizer Email M***********@p**.com
Narrative Pipeline booster pump had started pumping and went down due to seal failure. Employee went to investigate and found gasoline leaking from the seal area. Employee closed tank valve, esd the terminal, and contained product. Product stayed within the pump containment area and was cleaned up immediately. All proper notifications were made. Update requested per jocelyn kerl: the pump seal was replaced that day and put back into service. Updated 2/2/2015 due to amount of release reported incorrectly. First report as .38 bbls, correct amount is .90 bbls. 6/22/2015 there is no update just finalized report

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